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N57AT accident description

Alaska map... Alaska list
Crash location 64.647500°N, 145.878611°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect.
Nearest city Salcha, AK
64.547415°N, 147.012191°W
34.3 miles away
Tail number N57AT
Accident date 27 May 2017
Aircraft type Arctic Aircraft Co Inc S 1B2
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On May 27, 2017, about 1122 Alaska daylight time, an Arctic Aircraft Company S-1B2 airplane, N57AT, impacted terrain following a loss of control, about 35 miles east of Salcha, Alaska. The private pilot and the passenger sustained fatal injuries, and the airplane was substantially damaged. The airplane was registered to Brice Consulting LLC and operated by the pilot as a 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed, and no flight plan had been filed. The flight departed from an off-airport landing site near Fairbanks, Alaska, about 0925.

According to a family member of the pilot, the purpose of the flight was to search for an overdue boat that was piloted by a family member of the passenger with the intent of landing at a remote unimproved airstrip located near the boat's destination. The boat had left the previous evening for a recreational cabin located along the Salcha River.

During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) on June 1, 2017, a witness reported that she observed the airplane circle the remote unimproved airstrip along the Salcha River. While the airplane was circling, its nose suddenly dropped, and the airplane descended in a near-vertical attitude. She stated that the engine continued to run, and the airplane did not make any unusual sounds, other than an increase in engine rpm, during the descent. The witness reported strong wind conditions prevailed at the time of the accident.

PERSONNEL INFORMATION

The pilot, age 81, held a private pilot certificate with an airplane single-engine land rating. His most recent third-class medical was issued on September 30, 2015, with the limitation that he must wear corrective lenses.

Personal flight records were located for the pilot; however, they were not complete. The aeronautical experience listed in this report was obtained from a review of the Federal Aviation Administration (FAA) records for the pilot on file in the Airman and Medical Records Center located in Oklahoma City. The pilot did not report flight experience on his most current application for a medical certificate dated, September 3, 2015. However, on his application for a prior medical certificate, dated August 7, 2013, he indicated that his total aeronautical experience was about 1,960 hours of which 60 hours were in the previous 6 months.

AIRCRAFT INFORMATION

At the time of the accident, the 1978 model year airplane had a total time in service of 3,087.50 flight hours. A review of the maintenance records revealed that the most recent annual inspection of the airframe and engine was completed 27.10 flight hours before the accident on June 9, 2016.

The airplane was equipped with a 160-horsepower Lycoming O-320 B2B engine. At the time of the accident, the engine had accumulated 1,748.00 hours since overhaul.

METEOROLOGICAL INFORMATION

The closest official weather observation station to the accident site was Eielson Air Force Base, Fairbanks, Alaska, located about 35 miles east of the accident site. At 1058, Eielson was reporting, in part, wind calm; visibility 10 statute miles; clouds and ceiling 10,000 ft broken; temperature 52°F; dew point 27°F; and altimeter 30.04 inches of mercury.

WRECKAGE AND IMPACT INFORMATION

The wreckage was located in an area of black spruce trees and tundra-covered terrain at an elevation about 1,000 ft mean sea level. The on-scene examination revealed that the airplane impacted in a near-vertical attitude, and the nose of the airplane was on about a 110° magnetic heading.

All of the airplane's major components were found at the main wreckage site. The cockpit area was extensively damaged. The engine, firewall, and instrument panel were displaced upward and aft. The mixture control was found in the full-forward position, and the carburetor heat was in the off position.

The airplane's right wing remained attached to the fuselage. About 2 feet of the outboard portion of the right wing exhibited extensive leading edge aft crushing. The airplane's left wing separated from the fuselage at its rear attach point but remained attached at its forward attach point.

The left and right flaps remained attached to their respective attach points. The inboard portion of the right flap was crushed against the side of the fuselage and bent about 20° down. The left flap was relatively free of impact damage.

The horizontal and vertical stabilizer, elevators, and rudder remained attached to the empennage and were free of impact damage.

All the primary flight control surfaces were identified at the accident site, and flight control continuity was verified from the cockpit to the elevators and rudder. Aileron control continuity was established in the direct cables from the cockpit to the right aileron and from the cockpit through the point where the cable's turnbuckle was disassembled for recovery to the left aileron. In addition, aileron control continuity was established in the balance cable from the right and left ailerons to the point where the cable fractured with features consistent with tension overload.

The engine sustained impact damage to the front and underside. An examination of the engine did not reveal any anomalies, contamination, or evidence of malfunction in any of the engine accessories. Examination of the cylinders, pistons, valve train, crankshaft, and other internal components revealed no evidence of an anomaly or malfunction that would have precluded normal operation. Both magnetos were removed from the engine, and their couplings were rotated by hand. When each coupling was rotated, blue spark was observed at the distributor in rotational order.

The propeller remained attached to the engine crankshaft by 2 of the 6 attach bolts. One propeller blade exhibited substantial torsional "S" twisting and light chordwise scratching. The other propeller blade exhibited light chordwise scratching and aft bending about 3 inches from the tip.

The examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.

MEDICAL AND PATHOLGOICAL INFORMATION

The Alaska State Medical Examiner, Anchorage, Alaska, conducted an autopsy of the pilot on May 30, 2017. The cause of death was attributed to multiple blunt force injuries.

The FAA's Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma, performed toxicology testing on specimens from the pilot. The testing was negative for carbon monoxide and alcohol. The testing revealed unspecified levels of verapamil in the blood and liver and its active metabolite, norverapamil, in the blood. Verapamil is a prescription calcium channel blocker used to treat high blood pressure, angina, and arrhythmias.

TESTS AND RESEARCH

At the time of the accident, the pilot was using a Garmin Aera series portable global positioning system (GPS) receiver capable of storing route-of-flight data. The unit was sent to the NTSB's Alaska Regional Headquarters and data for the accident flight, which included, in part, time, latitude, longitude, and GPS altitude were extracted. Groundspeed and course information were derived from the extracted parameters.

The GPS data logs for May 27, 2017, revealed that the flight departed the remote off-airport landing site about 0925:30. After departure, the airplane proceeded southeast along the Tanana River before it turned east and proceeded up the Salcha River. The last fully recorded GPS data point was at 1122:39 when the airplane was at 1,705 ft (GPS derived altitude), heading 132° (true), and 47 knots ground speed.

A flight track map overlay and tabular data corresponding to the accident flight are available in the public docket for this accident.

ADDITIONAL INFORMATION

Estimated Weight and Balance

An estimate of the airplane's weight and balance at the time of the accident was calculated based on the following information.

The pilot's weight was taken from his most current FAA medical examination. The weight of the rear seat passenger was taken from his Alaska state driver's license.

In a telephone conversation with the NTSB IIC on July 26, 2017, the Alaska State Troopers who recovered two backpacks from the accident site estimated their total weight at 25 pounds, or about 12.5 pounds each.

During a conversation with the IIC, a family member of the pilot reported that fuel was not available at the remote landing site along the Salcha River. The fuel onboard at the time of the accident was estimated by calculating the amount of fuel required for the estimated 45-minute direct return flight from the accident site to the originating airstrip plus the required 30-minute reserve. Using an average fuel burn rate of 8 gallons per hour, the quantity of fuel in the airplane at the time of the accident was estimated to be 10 gallons.

A friend of the pilot provided the NTSB IIC with a list of items that were onboard the airplane at the time of the accident. Exemplar items were weighed, and those weights were used to compute the weight and balance.

The last documented weight and balance information located for the airplane was dated May 29, 2015. At that time, the basic empty weight of the airplane on wheels was 1,274.50 pounds with a center of gravity of 11.53 inches.

Basic Empty Weight– 1,274.50 pounds

Pilot– 184 pounds

Rear Seat Passenger – 170 pounds

24 pack water – 27 pounds

6 bottles wine – 17 pounds

Frying pan – 0.5 pounds

8 pack paper towels – 4 pounds

3 patio pillows – 3.5 pounds

2 backpacks – 25 pounds

Fuel (10 gallons) – 60 pounds

Oil (8 quarts) – 15 pounds

Using the values listed above, the gross weight of the airplane at the time of the accident was estimated to be 1,780.5 pounds, which was 130.5 pounds over the approved maximum takeoff gross weight for the airplane of 1,650 pounds. The estimated center of gravity at the time of the accident was 15.896 inches. The center of gravity range at 1,650 pounds (maximum gross weight) was 11.0 inches to 15.8 inches.

NTSB Probable Cause

The pilot's failure to maintain adequate airspeed while maneuvering in high winds, which resulted in the airplane exceeding its critical angle of attack and an aerodynamic stall. Contributing to the accident was the pilot's improper decision to load the airplane beyond its allowable gross weight and center of gravity limits.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.