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N62AK accident description

Alaska map... Alaska list
Crash location 58.335277°N, 135.066945°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect.
Nearest city Juneau, AK
58.301944°N, 134.419722°W
23.6 miles away
Tail number N62AK
Accident date 17 Jul 2015
Aircraft type Cessna 207A
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On July 17, 2015, about 1318 Alaska daylight time, a Cessna 207A airplane, N62AK, sustained substantial damage following an in-flight collision with tree-covered terrain about 18 miles west of Juneau, Alaska. The commercial pilot sustained fatal injuries, and four passengers sustained serious injuries. The flight was being operated as flight 202 by SeaPort Airlines, Inc., dba Wings of Alaska, as a 14 Code of Federal Regulations (CFR) Part 135 visual flight rules (VFR) scheduled commuter flight. (Wings of Alaska has been sold and is currently under different ownership.) Visual meteorological conditions were reported at the Juneau International Airport at the time of departure. A company flight plan had been filed, and company flight-following procedures were in effect. Flight 202 departed the Juneau Airport about 1308 for a scheduled 20-minute flight to Hoonah, Alaska.

On the day of the accident, the pilot arrived at the company office in Juneau about 1200. The accident flight was the pilot's first scheduled flight of the day. The company flight coordinator on duty at the time told the pilot that most flights to Hoonah were cancelled in the morning due to poor weather conditions and that one pilot had turned around due to weather. The flight coordinator said that the weather had started lifting around 1000 and that the first flight to Hoonah had departed at 1045. He suggested that the accident pilot talk with the pilot who had just returned. The dispatch group had a shift change between the time the accident pilot came on duty and when the pilot departed. The company flight coordinator on duty at the time of the accident only communicated with the pilot when she reported taxiing off the ramp for departure. No weather information was discussed, and no further radio communications were received from the pilot by the company.

According to Juneau Air Traffic Control Tower (ATCT) personnel, the pilot requested and received taxi clearance to depart for the 20-minute VFR flight to Hoonah at 1306. The flight was cleared for takeoff about 2 minutes later by the ATCT specialist on duty with no reported problems. About 15 minutes later, Juneau Police dispatchers received a 911 cell phone call from a passenger on board stating that the airplane had crashed.

During an interview with one of the surviving passengers, who was sitting directly behind the pilot, he stated that the pilot seemed normal during the preflight and briefing. After takeoff, the turbulence was heavy, and there were layers of fog and clouds and some rain. He had taken this flight numerous times and thought that the flight route that the pilot was taking was somewhat unusual. Before the impact, he thought that the pilot was trying to climb over the approaching mountain and skirt between a layer of clouds. He saw the trees coming at the windshield, and the pilot jerked back on the controls, and then he heard a "loud boom." The next thing that he remembered was sitting outside the airplane. He said that there were no unusual sounds from the engine and that the airplane appeared to be flying normally before the impact.

Automatic dependent surveillance-broadcast (ADS-B) data received by the Anchorage ATCT showed the following:

At 1308:09, the accident airplane took off from JNU.

At 1312:33, the accident airplane started a northwesterly turn around the west side of Portland Island at an ADS-B reported altitude of 825 ft mean sea level (msl).

At 1314:20, the accident airplane began a turn to a westerly heading at an ADS-B reported altitude of 825 ft msl.

At 1316:25, the accident airplane crossed the western shoreline of Admiralty Island at an ADS-B reported altitude of 675 ft msl and continued on a constant heading until the last ADS-B point was recorded.

The last ADS-B point was received at 1317:27, when the airplane was over Lynn Canal, about 1 mile from the eastern shoreline of the Chilkat mountain range at an ADS-B reported altitude of 525 ft msl. The last 30 seconds of the flight was missing from the ADS-B data.

PERSONNEL INFORMATION

The pilot, age 45, held a commercial pilot certificate with airplane single-engine land and sea, multiengine land, and instrument ratings. The pilot was issued a first-class airman medical certificate on April 9, 2015, with the limitation that she "must wear corrective lenses."

Company training records indicated that the pilot completed basic indoctrination on May 25, 2015, and initial ground training on June 2, 2015. Ground training curriculum was completed in two locations: Portland, Oregon, and Juneau. The pilot's most recent Part 135 proficiency checks (135.293 (a) (b) and 135.299) were completed in the Cessna 207 on June 12, 2015. Company records indicated that she had a total time of 840 flight hours.

The base chief pilot, who provided about half of the accident pilot's flight training, said that she was very good on systems but that she needed a few additional hours of flight training and initial operating experience before he was comfortable signing her off. He noted that the one thing that he really liked about her was that she wasn't afraid of turning around if she was uncomfortable. He did not notice any negative attitudes or habits with her flying.

The pilot's normal shift was the p.m. shift, which typically began at 1200 and ended at 2200. The pilot's flight and duty time records indicated that, the day before the accident, she flew 3.7 hours and then went off duty at 2200. The accident flight was the pilot's first flight of the day.

In June 2015, the pilot was on duty for 27 days, flew about 23 hours, and had 3 days off. In July 2015, the pilot was on duty for 11 days, including the day of the accident; flew about 41 hours; and had 6 days off. The pilot had not had a day off in the 72 hours preceding the accident flight. During that time, she flew a total of 19 flight segments, totaling 9.4 hours, not including the accident flight.

The pilot's roommates and family members reported no unusual activity in the 72 hours preceding the accident. However, in an interview with the pilot's sister, she said that the pilot had told her about an incident that had happened 2 or 3 weeks before the accident where she had gotten into a bad storm during a flight. The pilot said that she and her passengers were praying together to get through the weather and that eventually she saw the runway and was able to land the airplane uneventfully. Other than this event, the accident pilot never mentioned to her sister any concerns about flying for the company for which she worked.

AIRCRAFT INFORMATION

The accident airplane, a Cessna 207A, N62AK, was manufactured in 1984. Before the accident flight, the airplane had logged a total time in service of 26,613.1 flight hours. The airplane was maintained under a 100-hour/annual inspection program, and the most recent 100-hour inspection of the airframe and engine was on July 6, 2015.

The airplane was equipped with a Continental Motors IO-520-F 285-horsepower reciprocating engine. The engine was factory rebuilt on June 16, 2015; installed on the airplane July 14, 2015; and had accumulated about 8.2 hours of operation before the accident flight.

METEOROLOGICAL INFORMATION

The area forecast issued by the National Weather Service Alaska Aviation Weather Unit (AAWU) at 1210 included an AIRMET for mountain obscuration due to clouds and precipitation, and the AIRMET was valid at the accident site at the accident time. The area forecast mentioned scattered clouds at 1,200 ft msl with broken to overcast ceilings at 2,000 ft msl with cloud tops to flight level 250 and an occasional broken ceiling at 1,200 ft msl with 5 miles visibility and light rain. Isolated instrument flight rules (IFR) conditions were also forecast with rain and mist. The AAWU weather charts produced at 1200 indicated that the accident site was on the boundary of marginal VFR to IFR conditions with isolated moderate low-level turbulence between the surface and 6,000 ft msl.

The closest official weather observation station is Juneau, which is located about 18 miles east of the accident site. At 1253, a METAR was reporting, in part, wind 110° at 14 knots; visibility 7 statute miles in light rain and mist; clouds and ceiling 200 ft few, 3,500 ft overcast; temperature 57° F; dew point 55° F; altimeter 30.24 inches of Mercury.

Numerous Federal Aviation Administration (FAA) weather cameras are located in the vicinity of the Juneau Airport. Images from several of the cameras closest to the pilot's flight route were obtained for the period from 1100 to 1600 on the day of the accident. Figure 1 shows an image that was taken about 5 minutes before the estimated accident time, facing the direction of the accident location. (Refer to the Meteorology Group Chairman's Factual Report in the public docket for further weather information and weather camera images.)

No record was found indicating that the pilot used the company computer to review weather information before the flight nor of her having received or retrieved any weather information before the flight. The flight coordinator did not review weather camera images with the accident pilot before the flight and had no further communication with the pilot about the weather.

FLIGHT RECORDERS

The accident airplane was not equipped, nor was it required to be equipped with, a cockpit voice recorder or a flight data recorder.

WRECKAGE AND IMPACT INFORMATION

On-scene examination revealed that the airplane impacted a large spruce tree at an elevation of about 1,250 ft msl. After the initial impact, the airplane fuselage separated into two pieces. The forward section of the airplane, consisting of the cockpit and engine, separated just forward of the main landing gear assembly and came to rest inverted about 50 ft forward of the initial impact point; the cockpit survivable space was severely compromised. The remaining section, consisting of the main cabin, wings, and empennage, came to rest inverted just below the initial impact point. The wreckage path was on a magnetic heading of about 215° and oriented uphill. The trees surrounding the accident site were on average over 100 ft tall.

The wreckage was recovered from the accident site on July 20, 2015, and placed in a secure hangar at the Juneau Airport. The National Transportation Safety Board (NTSB) investigator-in-charge (IIC), FAA IIC, a Textron Aviation air safety investigator, and a party representative from the operator examined the airplane on July 20 and 21.

The fuselage and engine compartment forward of fuselage station (FS) 65.33 was separated from the main fuselage and was found inverted 50 ft from the main fuselage. Both crew seats were observed in the forward fuselage. The engine remained in the forward fuselage. Both wings remained attached to the main fuselage. The left pilot's door had separated from the fuselage and was in the trees. The right passenger door had separated from the forward fuselage. The forward section of the cargo door remained attached to the fuselage. The aft section of the cargo door was separated from the fuselage. The empennage remained attached to the main fuselage and exhibited tree impact damage from FS 168.0 to 210.6. The outboard section of the right horizontal stabilizer from stabilizer station (SS) 54.4 outboard was not found. A section of the right elevator from SS 35.9 outboard was separated from the elevator and found at the main impact site.

The left wing had a large tree impact mark near wing station (WS) 56.53, which displaced the leading edge back to the main spar and displaced the main spar aft about 10 inches. The flap and aileron remained attached to the wing.

The right wing had a tree impact mark near WS 85.62, which displaced the leading edge back to the main spar. The leading edge was damaged from right WS 136.00 to the tip. The outboard section of the right wing from WS 172.00 to the tip and aileron were displaced upward. The flap and aileron remained attached to the wing.

The aileron direct cable to the left wing was found with the ball end pulled out of the control pulley. The cable was continuous out to the left aileron bellcrank. The aileron crossover cable was continuous to the right aileron bellcrank. The right direct cable was continuous from the right aileron bellcrank to a tension overload separation in the doorpost area.

The elevator cables were attached to the elevator torque tube and extended to about FS 95.33 where they exhibited a tension overload type separation. The elevator cables were attached to the aft elevator bellcrank and extended forward to about FS 95.33 where they exhibited a tension overload type separation. The elevator trim cables exhibited a tension overload type separation. The elevator trim tab actuator rod was observed extended the full length of the rod, and when slightly turned, the rod separated from the actuator.

Both rudder cables were attached to the rudder bars in the cockpit and exhibited a tension overload type separation near FS 59.70. The aft section of each rudder cable was attached to the rudder, and the rudder actuated when the cables were moved.

The flap actuator was observed in the "up" position. The flap follow up/indicator cable was stretched during the accident sequence. The indicator was observed in the "full flaps down" position, and the flap handle was in the "10°" position. The cables from the left wing to the right flap were attached.

The fuel strainer was removed from the airplane, and it contained fuel. A sample could not be obtained due to the position of the strainer in the wreckage. Air was passed through both the left and right wing vent systems. Both fuel caps on both wings were observed installed on their filler necks, and their seals were pliable.

The restraint systems of both crew seats consisted of compatible Cessna and Air Carriers Interiors, Inc., Kent, Washington, parts. Both of the crew seats remained partially attached to the seat tracks. The pilot's seat was equipped with an SEB07-5 Pilot and Copilot Secondary Seat Stop Installation.

All the passenger seats were separated from the seat tracks. Rescue personnel removed some of the seats from the airplane during the rescue. Several of the passenger seats exhibited damage to the seat base and attachment feet.

No preaccident anomalies were noted with the airframe that would have precluded normal operation.

MEDICAL AND PATHOLOGICAL INFORMATION

The State of Alaska Medical Examiner, Anchorage, Alaska, conducted an autopsy of the pilot. The cause of death for the pilot was attributed to "multiple blunt force injuries."

The FAA's Civil Aerospace Medical Institute performed toxicological testing on specimens from the pilot on September 9, 2015, which were negative for carbon monoxide and ethanol. The toxicological testing detected Valsartan in the pilot's urine and blood. Valsartan is a prescription medication used to treat high blood pressure. The pilot reported the use of this medication on her last application for an airman medical certificate.

SEARCH AND RESCUE

About 1336, the US Coast Guard (USCG) in Alaska received a 406-megahertz emergency locator transmitter (ELT) signal assigned to the accident airplane. At 1421, after being notified of an overdue airplane and after learning about reports of an ELT signal along the accident pilot's anticipated flight route, search and rescue personnel from the USCG Air Station Sitka began a search for the missing airplane. About 1650, the crew of a USCG HH-60 helicopter located the airplane's wreckage in an area of mountainous, tree-covered terrain. A rescue swimmer was lowered to the accident site and discovered that the pilot had died at the scene and that the four other occupants had survived the crash. The four survivors were hoisted aboard the HH-60 helicopter in two trips and then transported to Juneau.

SURVIVAL ASPECTS

All four passengers in the main cabin survived the accident. After the initial impact, the fuselage section, consisting of the main passenger cabin, fell straight down the trunk of the tree and came to rest inverted. The cabin's structure remained relatively intact with sufficient survivable sp

NTSB Probable Cause

The pilot's decision to initiate and continue visual flight into instrument meteorological conditions, which resulted in a loss of situational awareness and controlled flight into terrain. Contributing to the accident were the company's failure to follow its operational control and flight release procedures and its inadequate training and oversight of operational control personnel. Also contributing to the accident was the Federal Aviation Administration's failure to hold the company accountable for correcting known regulatory deficiencies and ensuring that it complied with its operational control procedures.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.