Plane crash map Locate crash sites, wreckage and more

N888TP accident description

Arkansas map... Arkansas list
Crash location 35.896389°N, 93.760556°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect.
Nearest city Huntsville, AR
36.086187°N, 93.741303°W
13.2 miles away
Tail number N888TP
Accident date 21 Oct 2013
Aircraft type Piper Pa 32R-301
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On October 21, 2013, about 1406 central daylight time, a Piper PA-32R-301 airplane, N888TP, impacted trees and terrain during a descent from cruise near Huntsville, Arkansas. The pilot and passenger sustained fatal injuries. The airplane was destroyed. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Day visual flight rules (VFR) conditions prevailed for the flight, which did not operate on a VFR flight plan. The flight originated from the Thomas C Russell Field Airport (ALX), near Alexander City, Alabama, about 1045, and was destined for the Claremore Regional Airport (GCM), near Claremore, Oklahoma.

Flight service station records revealed that on October 20, 2013, the pilot representing N888TP obtained a preflight outlook weather briefing for a VFR flight departing on October 21, 2013, from ALX to GCM with an estimated time en route of four hours. On October 21, 2013, the pilot representing N888TP additionally obtained a preflight pilot briefing for a VFR flight departing at 1000 with an estimated time en route of four hours.

According to the fueling records, the airplane's fuel tanks were serviced with 57.74 gallons of aviation gasoline on October 18, 2013, at ALX. Following that fueling, a lineman at ALX helped load one suitcase, two hanging bags, and one set of golf clubs into a car. The pilot subsequently returned on October 21, 2013, and tried multiple times to start the engine. He was able to start the engine and the lineman indicated that the engine started without any "sputtering or popping." Additionally, the lineman did not see any black smoke during the engine start.

A mechanic at ALX observed the passenger and pilot board the aircraft without the pilot making a pre-flight inspection, which he thought was unusual since the aircraft had been tied down over the weekend and had sat in the rain. He then observed the pilot make numerous attempts to start the engine, "which almost completely drained the battery." The pilot was able to get the engine started without an external power source. The mechanic then observed him taxi out to the runway and depart runway 18 without ever doing a run up and/or magneto check."

The pilot was en route to GCM where he requested and was given VFR flight following. According to a transcript of recorded communications involving the Federal Aviation Administration (FAA) Razorback East radar approach control frequency, the pilot checked on with an approach controller about 1354. The controller advised the pilot of the current local altimeter setting and queried his altitude. The pilot replied he was at 5,800 feet. About 1357, the pilot advised the controller that the flight was descending to 4,500 feet.

At 1357:42, the controller said, "november nine eight eight tango papa roger maintain v f r altitude your discretion i'm showing moderate to to heavy rain uh at your twelve o'clock and approximately uh two

miles it's uh just south along your route of flight and then there's a heavier area uh approximately fifteen miles uh west along your route of flight."

At 1358:01, the pilot replied, "eight eight eight tango papa v f r."

At 1404:18, the controller said, "november eight eight eight tango papa the uh weather that i'm showing is at your twelve o'clock and er precipitation returns are just at your twelve o'clock and about uh six miles uh about eight miles into that it uh uh is showing um heavy precipitation that's uh developing and building uh to the east."

At 1404:38, the pilot replied, "roger eight eight eight tango papa reckon we oughta do a one eighty."

At 1404:43, the controller said, "no sir eight eight eight tango papa if you uh take you to the north if you'd like vectors through it suggest heading three five zero towards huntsville and then once you get uh just uh west of huntsville i can turn you back to the west.

At 1405:54, the pilot replied, "alright eight eight eight tango papa three five zero."

At 1405:34, the controller said, "lance eight tango papa fly heading three six zero i'm going to leave you north bound for about uh five miles then i'll turn you back to the north west to get you clear of that weather."

At 1406:47, the pilot replied, "three six zero eight tango pop."

The controller queried the flight and no further transmissions from the accident pilot were recorded. The transcript is appended to the docket material associated with this investigation.

The airplane was observed on radar to descend at a high rate of speed following the turn and the Madison County Sheriff's Office was subsequently advised of coordinates for a possible airplane down. A search was conducted and responders using an emergency locator transmitter detector located the wreckage about 0845 on October 22, 2013.

PERSONNEL INFORMATION

The pilot held a FAA private pilot certificate with an airplane single engine land rating which was issued on April 25, 2013. The pilot took an initial check ride for his private pilot certificate on April 21, 2013. He did not pass that check ride and was given a notice of disapproval of application. The pilot was subsequently reexamined on the areas failed on that check ride, which were takeoffs, landings, and go-arounds, slow flight and stalls, and emergency operations. He held a FAA Third Class Medical Certificate dated January 23, 2013, with a limitation to wear corrective lenses. The pilot reported on the application for that medical certificate that he had accumulated 45 hours of total flight time and 5 hours of flight time in the previous six months. The pilot reported to his airplane's insurance company that he had accumulated 204 hours of total flight time and accumulated 16 hours of flight time in the PA-32R-301 as of October 3, 2013. According to the pilot's logbook, he recorded that he had accumulated 224.7 hours of total flight time, 8.1 hours of simulated instrument flight time, 1.9 hours of actual instrument flight time, and 36.1 hours of flight time in the same make and model airplane as the accident airplane.

AIRCRAFT INFORMATION

N888TP was a 1997 Piper PA-32R-301 airplane with serial number 3246090. The airplane was a low-wing, all-metal, single-engine, six-place monoplane. It had a retractable tricycle landing gear configuration, and was powered by a fuel injected, six-cylinder, Lycoming IO-540-K1G5 engine, bearing serial number L-26058-48A, and was marked as producing 300-horsepower at 2,700 rpm. An airplane logbook endorsement showed that the airplane's last annual inspection was completed on September 16, 2013, and that the airplane had accumulated 2,325.3 hours of total time.

METEOROLOGICAL INFORMATION

A National Transportation Safety Board (NTSB) senior meteorologist reviewed weather documents to include flight service station briefings given to the pilot representing N888TP. Those briefings indicated the pilot should expect VFR conditions to prevail along the route of flight with no significant flight restrictions. The meteorologists review revealed that National Weather Service (NWS) surfact analysis for 1300 depicted a cold front over the planned route of flight and immediately east of the accident site. The chart depicted overcast clouds with light continuous rain behind the front.

The NWS National radar mosaic for 1400 depicted a band of weather echoes from southern Missouri southwestward across northern Arkansas into eastern Oklahoma. The band of echoes was along the route of flight and over the accident site.

The closest weather reporting location, about 21 miles and 289 degrees from the accident site, at the Drake Field Airport (FYV), near Fayetteville, AR, reported a wind shift associated with the cold front passage with marginal VFR (MVFR) to temporary instrument flight rules (IFR) conditions in light to moderate rain behind the front. At 1353, the recorded weather at FYV was: wind calm; visibility 5 statute miles; present weather rain, mist; sky condition scattered clouds 800 feet, broken clouds 1,800 feet, overcast clouds 5,000 feet; temperature 10 degrees C; dew point 9 degrees C; altimeter 30.08 inches of mercury. The next closest reporting stations at the Springdale Municipal Airport, near Springdale, and the Boone County Airport, in Harrison, Arkansas, both reported VFR conditions with broken to overcast sky conditions with surrounding light rain.

The North American Mesoscale model sounding for 1300 over the accident site indicated a potential cloud base at 1,000 feet above ground level. The sounding was stable and supported nimbostratus type clouds capable of producing rain showers.

The Geostationary Operational Environmental Satellite (GOES) no. 13 infrared satellite imagery at 1402 depicted an extensive band of low to mid-level clouds over the region associated with the frontal system. The GOES-13 visible image for 1402 also depicted an overcast cloud cover over the accident site with nimbostratus type clouds. The satellite and radar imagery, and lightning data did not identify any cumulonimbus clouds or thunderstorms in the immediate vicinity of the accident site.

The NWS Weather Surveillance Radar 0.5 degree base reflectivity images for 1401 and 1407 depicted a band of light to moderate intensity echoes approximately 15 miles wide along the flight track. Over the accident site, the echo intensity was only 20 to 25 dBZ or light intensity echoes. The reflectivity images did not identify any strong convective echoes along the flight path of the accident airplane.

A review the lightning network indicated that there were no in-cloud or cloud-to-ground lightning activity in an approximate 20 mile radius and a 45 minute period surrounding the time of the accident.

The NWS Terminal Aerodrome Forecast (TAF) for FYV available at the time of preflight planning expected VFR conditions prevailing with a broken ceiling at 4,000 feet and light rain showers. The TAF for Tulsa International Airport, closest forecast to the destination, also expected VFR conditions to prevail with rain showers and a ceiling broken at 5,000 to 6,000 feet.

The NWS Area Forecast for the route forecast expected broken clouds at 6,000 feet above mean sea level with tops to 20,000 feet with isolated rain showers. The forecast was consistent with the TAFs issued across the region. There were no amending Airmen's Meteorological Information (AIRMET) for IFR conditions. No advisories were current for any large areas of IFR conditions or thunderstorms across the region. The Senior Meteorologist's Factual Report is appended to the docket associated with this investigation.

WRECKAGE AND IMPACT INFORMATION

The airplane wreckage was found about 13 miles south of Huntsville, Arkansas. It was situated about 1.4 miles and 305 degrees from the intersection of Madison County Road 5320 and Arkansas Highway 23. The wreckage was fragmented in an area that was tree covered, hilly, and had rocky terrain. The first observed impact to trees was found below the crest of a hill and the wreckage debris path extended down the hill about 450 feet to the hill's base. The debris pattern exhibited a general heading of approximately 255 degrees from the initial tree impact. Trees that were struck during the impact sequence exhibited witness marks to include broken branches, uprooted bases, and toppled over trunks in the direction of the debris pattern.

A postaccident on-scene investigation was conducted. All major components of the airplane were accounted for at the accident site. The left wing and right wings were fragmented during the impact sequence. Components from both wings to include their wingtip, aileron, flap, landing gear, and control cables were found along the debris field. All damage and separations were consistent with overload. Control cable separations exhibited a broomstrawed appearance consistent with overload separation. All fuel tanks were fragmented and no fuel was noted. Trees and ground areas exhibited discoloring and charring consistent with post impact ground fires.

The empennage was found fragmented along the debris path. The largest section consisted of sections of the horizontal stabilator, vertical stabilizer, and the lower portion of the rudder. The left side of the stabilator and outboard portion of the right side were separated and were found along the debris path. Both stabilator control cable attach fittings were noted. One cable had separated from the swaged ball on the end of the cable and the other cable had a broomstrawed separation. Both rudder cables were secure to the rudder bellcrank and continuous to the forward fuselage area where both had broomstrawed separations. The stabilator hinge and stop bolts were in place and secure. The balance tube was in place with weights secure. The rudder bellcrank was partially separated from the rudder. The lower hinge bolt and stop bolts were in place and secure. The pitch trim drum showed three threads upper extension, which would have been consistent with a trim tab position of about two degrees of the available five degrees nose down trim. The fuselage was fragmented by multiple impacts with trees and terrain. Airplane fuselage parts and contents to include seats, instrument panels, luggage, window and door openings, and control cables were found along the debris path. The instrument panel's instruments were fragmented. The airspeed indicator's face was the only remaining instrument in the panel and its needle was resting near 200 knots.

The engine was separated from its engine mount and the engine was found near the bottom of the hill by the end of the debris path. The propeller and the rear-mounted accessories were separated from the engine. Both magnetos were found in the debris path. One magneto exhibited spark when its impulse coupling was rotated by hand. The other magneto did not produce spark when rotated by hand and disassembly revealed a separation in the distributor gear. That gear separation was consistent with impact damage. The engine crankshaft was rotated using a pry-bar and the crankshaft's continuity was verified. The camshaft gear was also rotated by pry-bar and movement of some of its valves was observed. Impact damage to some push rods precluded full camshaft rotation.

Portions of the propeller hub and its two retained blades were buried in the ground with a tree trunk covering one blade. One blade was separated from the hub and the blade was found down the hill in the debris path. The propeller blades exhibited s-shaped bending. The propeller attach studs remained in the crankshaft flange. The propeller hub boltholes were deformed in a pattern that was opposite the direction or rotation.

No airframe or engine pre-impact anomalies were detected that would have precluded normal operations.

MEDICAL AND PATHOLOGICAL INFORMATION

The Medical Examiner Office at the Arkansas State Crime Laboratory performed an autopsy on the pilot on October 24, 2013. The cause of death was listed as blunt force injury.

The FAA Civil Aerospace Medical Institute prepared a Final Forensic Toxicology Accident Report on specimens from the pilot's autopsy. The report was negative for the tests performed.

NTSB Probable Cause

The noninstrument-rated pilot’s continued flight into an area of known rain with reduced visibility and his failure to maintain airplane control while maneuvering the airplane after entering these conditions.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.