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N391V accident description

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Crash location 33.970556°N, 112.695000°W
Nearest city Wickenburg, AZ
33.968641°N, 112.729622°W
2.0 miles away
Tail number N391V
Accident date 02 Nov 2013
Aircraft type Rovey Jason H RV-8
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On November 2, 2013, at 1141 mountain standard time, an experimental Rovey Vans RV-8 airplane, N391V, made a forced landing following an engine vibration and partial loss of engine power near Wickenburg, Arizona. The owner/builder/pilot operated the airplane under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. The pilot, the sole occupant, was not injured. The airplane sustained structural damage to the left wing and firewall. Visual meteorological conditions prevailed for the local area flight, and no flight plan had been filed. The flight originated from the Wickenburg Municipal Airport (E25), Wickenburg, about 1100 the day of the accident.

According to the pilot, he was a participant in a Sport Air Race League cross-country, in which participants raced against the clock. It was a 130-mile course, which departed from, and concluded at, Wickenburg Municipal Airport. The pilot stated that he was about 13 miles west of E25 at 1,200 feet agl, at maximum power and rpm, when he felt an immediate and sustained vibration, which he thought was from the engine or propeller. He radioed a mayday and stated that the airplane started to slow down. He was not able to land on United States (US) highway 60, in either direction, due to traffic. The pilot stated that he turned for Forepaugh Peak Road to make the forced landing. About 150 feet agl, he realized the airplane would not glide far enough to reach the road, and landed the airplane on the desert floor. After traveling through desert vegetation/brush, the airplane came to a stop in a nose down attitude.

The pilot reported that following the forced landing, he borrowed a club propeller and bolted it to his engine. He performed a ground run of the engine with no mechanical problems encountered. The engine was disassembled at a repair station in order to perform the propeller strike inspection, followed by an engine rebuild; there were no mechanical anomalies encountered.

The propeller hub was removed and examined at Ottoeson, Phoenix, Arizona, under the auspices of a Federal Aviation Administration (FAA) inspector. According to the FAA inspector, there was evidence at the hub of loading on the propeller at impact. He further reported that the propeller pins do not normally break off in accidents involving propeller strikes; however, the accident propeller pin had broken. According to engine performance downloads, it appeared that the propeller pin broke during flight.

TESTS AND RESEARCH

The propeller blades, hub case, and hub bearings were shipped to the National Transportation Safety Board (NTSB) metallurgical laboratory in Washington, D.C., for further examination. The hub had been disassembled prior to arrival at the metallurgical laboratory. The bearing and hub surfaces were generally in good condition with no abnormal signs of wear or pre impact damage. The propeller blades exhibited gouging and scratches along the longitudinal axis of the blade, with the blade tips damaged, primarily on the leading edges. According to the specialist, the witness marks were consistent with ground impact damage. One of the pitch change pins had fractured from the hub face, along the bend radius where the face and pin mate.

According to the specialist, the pin fracture surface had been damaged by smearing; however, the mating side fracture surface on the hub face was generally undamaged. The crack arrest and ratchet marks indicated progressive cracking, about 70 percent of the fracture surface. The specialist reported that the fatigue crack initiation site had multiple surface crack initiation sites. The surfaces of both the pin and the hub exhibited a dimpled pockmarked texture consistent with shot peening. The primary fatigue crack initiation site corresponded to a surface depression. A chemical composition was performed using the energy dispersive x-ray spectroscopy (EDS) and x-ray fluorescence (XRF), as well as hardness testing; there were discrepancies with the chemical or material composition. A detailed report is attached to the docket for this accident.

NTSB Probable Cause

The fatigue failure of a propeller pitch change pin due to excessive shot peening of the pin’s surface during the manufacturing process.

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