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N2052L accident description

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Crash location 37.858889°N, 120.166667°W
Nearest city Groveland, CA
37.838261°N, 120.232689°W
3.9 miles away
Tail number N2052L
Accident date 10 May 2016
Aircraft type Beech B24R
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On May 10, 2016, about 1215 Pacific daylight time, a Beech B24R Sierra, N2052L, was substantially damaged when it impacted terrain during an attempted departure from Pine Mountain Lake Airport (E45), Groveland, California. The pilot and the passenger/owner received minor injuries. The personal flight was conducted under the provisions of Title 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed.

The passenger, who was a student pilot, recently purchased the airplane in an estate sale. Both the pilot and owner lived in Mississippi, and had traveled to E45 to retrieve the airplane, and fly it back to Mississippi. The airplane was domiciled at E45, and had not been maintained, operated, or flown in over 10 years. Subsequent to his purchase, the new owner contracted with a mechanic at E45 to conduct maintenance on the airplane, in preparation for the flight to Mississippi.

The day prior to the accident, both fuel tanks were filled, and the pilot and owner took the airplane for its first flight after its dormant period. The airplane departed on runway 27, and flew one circuit in the airport traffic pattern, as planned. That flight was uneventful. The next day, the pilot and owner planned to again fly the airplane, this time departing the area for some systems evaluations, before returning to E45. This takeoff attempt, which terminated in the accident, was conducted on runway 9. The pilot reported that the first part of the takeoff roll and liftoff "appeared normal but during or at gear retraction the aircraft started losing power." He stated that with about 1,000 feet of runway remaining, the engine "was not producing enough power to climb or accelerate," and that it was apparent the airplane was not going to clear the trees beyond the runway end. The pilot focused on attempting to climb, while simultaneously avoiding a stall.

The airplane struck trees and a utility pole, and then thick underbrush and the ground. The airplane came to rest about 1,800 feet beyond the end of the runway, at a point slightly north (left) of the extended runway centerline. The fracture-separated outboard right wing was located adjacent to the utility pole, and the engine had separated from the fuselage. The fuselage was slightly crumpled and otherwise deformed, but the cabin retained its normal occupiable volume. There was no fire.

PERSONNEL INFORMATION

Pilot

The pilot reported that for both flights, he was seated in the left front seat, and was the sole manipulator of the controls. He held an airline transport pilot certificate, and reported about 22,800 total hours of flight experience, including about 4,310 hours in single engine airplanes. Prior to his flight in the airplane the day before the accident, the pilot had no experience in the accident airplane make and model. His most recent flight review was completed in May 2015, and his most recent Federal Aviation Administration (FAA) third-class medical certificate was issued in January 2015.

Owner

The owner was seated in the right front seat for both flights. He reported that he held a student pilot certificate, but had no experience in the accident airplane make and model, and was only an observer on the two fights.

Mechanic

The individual who conducted the maintenance on the airplane for the new owner, and who most recently made entries in, and signed, the airplane maintenance records, resided and had a hangar at E45. He also owned and operated a repair facility, Buchner Aircraft Specialties, at Fresno Chandler Executive Airport (FCH) in Fresno, California. According to FAA records, the individual had previously held a mechanic certificate, with Airframe, Powerplant, and Inspection Authorization (IA) ratings. However, during the period when the mechanic performed the maintenance on the accident airplane and returned it to service, his IA rating was not valid, due to its expiration more than a year prior.

FAA regulations require that IA ratings be renewed biennially, or they become invalid. One renewal method allows the applicant to take approved classes within a specified period near the end of their biennial period. If an applicant fails to renew in that manner within the designated timeframe, they must take specified FAA tests to re-validate their IA rating.

In March 2015, for undetermined reasons, the mechanic did not renew his IA rating within the designated period. He then attempted to re-validate his IA rating by taking the required FAA tests, but he did not successfully pass them; thus his IA rating remained expired/invalid.

AIRCRAFT INFORMATION

FAA information indicated that the airplane was manufactured in 1976, and was equipped with retractable landing gear, and a Lycoming IO-360-A1B6 series engine. The engine drove a constant-speed, two-blade propeller. The airplane's most recent FAA registration expired in 2011.

Excluding the maintenance conducted just prior to the accident, the most recent annual inspection had been completed in December 2005.

METEOROLOGICAL INFORMATION

E45 was not equipped with any official weather sensing or recording equipment. Resident and eyewitness reports indicated that about the time of the accident, the temperature was about 75 degrees F (23 C), and there was a light wind from the west. An individual who was a flight instructor and FAA-designated pilot examiner estimated that the tailwind component along runway 9 was about 5 knots.

Calculations using the available information indicated that the temperature was about 14 degrees C above the standard atmosphere value ("ISA"), and that the resulting density altitude was 4,686 feet.

AIRPORT INFORMATION

E45 was situated at an elevation of 2,933 feet above mean sea level, and was equipped with a single paved runway designated 9/27, which measured 3,624 ft by 50 ft. The western-most 1,000 ft segment of the runway was relatively level, but then the runway sloped uphill beyond that (towards the east). The slope of that uphill portion was not constant; a maximum up slope of 1.8 per cent was present for the segment between 2,500 and 3,000 ft from the threshold of runway 9. The overall average gradient was 1.1 per cent.

There was a 100 ft gravel overrun at the east end of the runway. Beyond that, the terrain descended about 30 feet, but that region was populated with numerous trees as high as about 100 feet.

WRECKAGE AND IMPACT INFORMATION

FAA inspectors examined the wreckage the day after the accident, before it was recovered. The airplane struck several trees and came to rest upright, in dense undergrowth. The cabin and fuselage remained relatively intact, which afforded protection for the occupants during impact. Both wings sustained significant impact damage, but remained attached to the fuselage. The left wing remained securely attached. The right wing was partially fracture-separated at the wing root, and its outboard end was fracture-separated; it was found at the base of the power pole that was struck about 20 feet agl. The ailerons and flaps remained attached to their respective wings. The right fuel tank was breached, but the left tank was full of fuel. The vertical stabilizer remained securely attached to the aft fuselage, and the rudder remained securely attached to the vertical stabilizer. The stabilator remained securely attached to the aft fuselage, and the pitch trim tab remained securely attached to the stabilator.

The engine was fracture-separated from the airframe, and came to rest inverted, about 10 feet ahead of the airplane. Both blades of the propeller remained securely installed in the propeller hub, and the hub remained attached to the engine.

All components of the airframe were accounted for, and were located in the debris path, or on or near the airplane. A detailed examination of the recovered wreckage was conducted a few weeks after the accident. There was no evidence of any in-flight or post-accident fire. No evidence consistent with any pre-impact malfunctions or failures of any airframe components that would have precluded continued normal operation was observed.

The fuselage had been cut for recovery, but flight control continuity was established for all flight controls. The cockpit stabilator trim tab indicator was observed to be set within the normal takeoff range. The stabilator trim actuator extension measurement was consistent with a stabilator trim tab position of 10º training edge down. However, because the fuselage had been cut and otherwise disturbed for the recovery, these values could not be considered to represent the takeoff pitch trim setting.

Witness marks on both sides of the fuselage, and on the inboard ends of both flaps, indicated that the flaps were in the retracted position at the time of impact. This was corroborated by flap jackscrew extension and cockpit position indicator information. The cockpit flap control was a momentary paddle-type switch, and the flap position indicator was a circular display with a face diameter of about 1 inch. Both were situated on the right side instrument sub-panel, just to the right of the center-mounted engine control quadrant.

Damage patterns were consistent with the landing gear being near- or fully-retracted at the time of impact; the three landing gear were essentially undamaged. The landing gear control handle was in the UP position.

The airspeed indicator was properly marked; the colored speed arcs were in accordance with the Pilot's Operating Handbook (POH) values.

All three engine control (throttle, mixture, and propeller) push-pull cables had been fracture-separated from their respective engine components, at locations forward of the firewall; all three exhibited continuity from the cockpit control to the fracture locations forward of the firewall.

The fuel boost pump switch was set to the OFF, and the fuel selector valve was set to the right tank. Detailed examination of the airframe fuel system, including operation of the fuel boost pump and internal inspections of all components, did not reveal any indications of any pre-impact anomalies or deficiencies that would have precluded normal operation.

The engine bore no evidence of any pre-impact damage or failures. The engine-driven fuel pump was fracture-separated from the engine. The pump diaphragm was intact, and the engine actuator lever functioned with engine rotation. The fuel flow divider (distribution valve) and the fuel servo internal components were generally clean and intact. All lines and fittings were found to be secure. The spark plugs were new. Manual rotation of the engine resulted in thumb compression at all cylinders, in the proper sequence.

Both magnetos remained securely attached to the engine, but the left magneto bore impact damage. Magneto to engine timing was found to be 20 degrees for the right magneto, and 27 degrees for the left magneto. The Lycoming-specified timing is 20 degrees.

Both magnetos tested satisfactorily to rpm levels above the specified maximum rpm value of 2,700 for that engine/airframe combination. One harness lead exhibited an electrical short; any short would have manifested itself as engine roughness during the pilot's magneto check, but he did not report any such roughness. The cause/source of the short was not determined.

Aside from Airworthiness Directive (AD) 2015-19-07 (see below), the airplane, engine, magnetos, and fuel servo appeared to be in compliance with all applicable ADs.

The condition of the airframe and engine were not consistent with an airplane that had been subjected to a thorough annual inspection, and the requisite maintenance for a return to service. Items that were found to be non-conforming to the complete performance of an Annual or 100 Hour inspection and return to service included:

- Age hardened, deteriorated fuel injector line support clamp cushions, not in compliance with AD 2015-19-07 per Lycoming Service Bulletin 342G

- Uncleaned fuel injector nozzles (evidenced by sooty, partially-obstructed air bleed screens)

- Re-used, un-annealed M-674 spark plug gaskets

- Spark plug 2T found installed finger-tight

- Severely deteriorated internal muffler baffling

- All (except propeller governor) non-metallic flexible fuel and oil pressure hoses were over 40 years old

- Fuel cap external and internal seals age-deteriorated and cracked

- Fuel strainer gaskets age-deteriorated and cracked

ADDITIONAL INFORMATION

Mechanic and Maintenance Record Information

According to the pilot and the owner, a few weeks prior to the accident, the owner had contracted with a mechanic at E45 to conduct an annual inspection on the airplane, and to perform the maintenance necessary to render the airplane airworthy for its return to service. They also reported that subsequent to the maintenance, and prior to the accident flight, the mechanic made airframe and engine logbook entries that indicated that the airplane had been inspected in accordance with an annual inspection, was in airworthy condition, and that the mechanic's signature block denoted that he was an IA. Subsequent to the accident, the mechanic refused to provide the logbooks to the owner. The mechanic claimed that the owner owed him $6,000 for the maintenance that he had performed, and that he was retaining the logbooks for security until he was paid.

FAA and NTSB attempts to convince the mechanic to release the logbooks to the FAA or NTSB were unsuccessful; again the mechanic stated that he was holding the logbooks as security until he was paid by the owner. The mechanic eventually allowed an FAA inspector to examine and photograph the two most recent entries in each logbook. The FAA inspector, and his photographs, indicated that portions of the original airframe and engine logbook entries by the mechanic had been altered with "whiteout" and overwritten. The revised airframe and engine entry text indicated that the airplane had been inspected in accordance with a "ferry inspection," and the revised mechanic's signature block indicated that he was an "A&P."

"Ferry inspection" is not a term that is defined, referenced, or otherwise recognized by the FAA.

FAA and NTSB conversations with other aircraft owners at E45 revealed that subsequent to March 31, 2015, the mechanic had continued to represent himself as a valid IA holder, and that he had conducted and signed off numerous aircraft as an IA.

Airplane Performance

Takeoff performance distance data (ground roll, and total over 50 ft obstacle) for the airplane were presented in table form in the POH. The performance table values were predicated on the following fixed conditions:

- Gross weight: 2,750 lbs

- Engine/propeller rpm: 2,700

- Engine leaned "to field elevation"

- Flaps: 15º

- Landing gear retracted after lift-off

- Runway: paved, level, dry surface

- Takeoff speeds: lift off, 71mph; 50 ft height, 75 mph

The table provided for variations in the following parameters:

- Headwind (no tailwind accountability)

- Pressure altitude

- Ambient temperature

Because the POH performance data did not account for runway slope, tailwind, or 0º flaps, the manufacturer provided calculated performance estimates that accounted for variations in those parameters for two example cases. The first case used the prescribed takeoff flap setting of 15º, and the second used the actual takeoff setting of 0º. Both cases use the calculated pressure altitude, a 1.1% runway upslope, a 5 knot tailwind, and all other fixed parameter values specified above.

The 15º flap case resulted in an estimated ground roll distance of about 1,900 ft, and an estimated distance to 50 ft agl of about 3,250 ft. The 0º flap case resulted in an estimated ground roll distance of about 2,300 ft, and an estimated distance to 50 ft agl of about 3,700 ft. It should be noted that these results do not represent certificated performance, and should not be construed as such.

The pilot estimated that the airplane actually weighed about 2,460 lbs for the takeoff. Although the POH performance table included a "NOTE" that provided a means to account for weights below 2,750 lbs, there was insufficient data to substantiate application of that correction factor to these two perfo

NTSB Probable Cause

The pilot's decision to conduct an upslope, downwind takeoff combined with an improper flap setting, which resulted in the airplane's inability to clear trees beyond the runway end. The reason for the improper flap setting could not be determined.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.