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N902CS accident description

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Crash location 36.662778°N, 121.606111°W
Nearest city Salinas, CA
36.677737°N, 121.655501°W
2.9 miles away
Tail number N902CS
Accident date 21 Jul 2008
Aircraft type MD Helicopters Inc MD 902
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On July 21, 2008, at 1207 Pacific daylight time, an MD Helicopters, Inc., MD 902, N902CS, made a hard landing following a loss of anti-torque control at the Salinas Municipal Airport (SNS), Salinas, California. California Shock Trauma Air Rescue, d.b.a. CALSTAR, operated the helicopter under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91 as a positioning flight when the accident occurred. The pilot and two flight nurses were not injured; there was no patient on board. The helicopter sustained minor damage to the skids. The flight departed from the San Jose Regional Medical Center (RMC) helipad with a planned destination of SNS. A company visual flight rules (VFR) flight plan had been filed.

According to the pilot, the helicopter was on a 1-mile final when he noted that he was using more left pedal than he thought was necessary for the flight profile. He requested and received permission from SNS tower personnel to perform a right 360-degree turn, and then continue on to the CALSTAR ramp. Once the turn was completed, he continued on with his intended landing spot, as everything appeared normal. The pilot brought the helicopter to an 8- to 10-foot hover, the nose broke to the right, and the helicopter started an uncommanded right spin. He reported that full left pedal had no affect on stopping the spin. He then performed a hovering autorotation per the rotorcraft flight manual (RFM) while simultaneously rotating both twist grips to idle power. The helicopter landed hard, bounced, and came to rest about 45 degrees to the right of the first touch down point.

WITNESS STATEMENTS

According to the flight nurses, as the helicopter approached the airport, the pilot radioed the tower and requested a 360-degree turn before heading to the ramp. The 360-degree turn was normal. The pilot then proceeded to the CALSTAR ramp, and the pilot performed a right turn. They noted that the helicopter slowed, and started a flat right turn. The pilot reported that he had a stuck pedal and to hold on. The nurses reported several rotations before the helicopter landed hard, bounced back into the air, and then came to rest without further incident.

AIRCRAFT INFORMATION

The 2007 MD Helicopters, Inc., MD902 Explorer, serial number 900-00123, was powered by twin engine turboshaft Pratt and Whitney (P&W Canada) PW207E engines. According to CALSTAR, the helicopter had a total airframe time of 55 hours at the time of the accident. Engine number 1, serial number PCE-BG-0073, had a total of 85 hours. Engine number 2, serial number PCE-BG-0072, had a total of 84 hours. An annual inspection had been performed on June 11, 2008.

A Federal Aviation Administration (FAA) airworthiness inspector responded to SNS to examine the helicopter. He, along with CALSTAR maintenance personnel, found that the aft end of the rotating control cable (forward directional control cable, part number 900C3010045-105) had failed where the threaded section of the control cable threads into the rotating cone (control rod part number 900C2010582-103). The part and associated hardware were shipped to the National Transportation Safety Board’s (NTSB) Materials Laboratory, Washington, D.C., for further examination.

NOTAR Anti-Torque System

The helicopter is equipped with the NOTAR system for anti-torque and directional control (the NOTAR [no tail rotor] system is exclusive to MD helicopters). A variable pitch fan driven by the engines inducts ambient air and pressurizes the tail boom with low pressure, high volume air. Operation of the control pedals rotates a cone located at the rear of the tail boom and also varies the pitch of the fan. When the helicopter is in a hover, some of the air in the tail boom is expelled through longitudinal slots on the right side to produce sufficient lift to provide a majority of the anti-torque required. The remaining air is utilized for directional control and is expelled sideways through a thruster located at the rear of the tail boom. The rotating cone is located over the thruster and governs the amount of air expelled. In forward-flight, vertical fins located at each end of a horizontal stabilizer, forward of the rotating cone, provide a majority of the anti-torque and the thruster still provides the directional control. The components received are part of the control system for the rotating cone.

TESTS AND RESEARCH

A Safety Board specialist examined the forward directional control cable and the rotating cone control rod of the NOTAR assembly. Documents reviewed were the MD Helicopters maintenance manual CSP-900-RMM-2 section 67-20-00; the illustrated parts list CSP-900IPL-4, section 67-20-00; the National Aerospace Standard (NAS) 1193, locking device, positive index; McDonnell Douglas Helicopter Company drawing 900C3010045-105, cable assembly, forward directional controls; and the Aerocontrolex drawing 2601624, end rod.

The forward directional control cable is connected to the rotating cone control rod, and makes up the directional control rod assembly. A two-part locking device, identified in the illustrated parts list as a locking device positive index part number NAS1193K4CP, was located between the components on the threaded portion near the aft end of the control cable. One part has an internal tang intended to be engaged in a groove in the threaded section of the aft end of the control cable and radial serrations on the face that engages with the second part. The second part has a serrated face to mate with the first part and castellations on the other face that engage with slots in the forward end of the rotating cone control rod. The second part also has an external tang, with a wire locking hole. Proper engagement of the castellations and serrations is required when the telescopic part of the control cable is rotated toward the rotating cone control rod during assembly. The assembly is then torque loaded and the telescoping end is wire locked to the external tang of the locking device. The grooves in the aft threaded portions of the control cable were found offset by approximately 45 degrees.

The Safety Board specialist examined the aft threaded end of the control cable that was protruding from the telescope part and noted that it had been mechanically damaged and was too short to engage with the rotating cone control rod. The remaining portion of the thread was found still located in the end of the rotating cone control rod with a relatively undamaged fracture face. The forward face of the rotating cone control rod also displayed a radially oriented shallow groove consistent with the castellations on the locking device being positioned on the face during assembly and not in the grooves provided for that purpose. Circumferential marks extended from the outer tips of the shallow groove consistent with the locking device rotating. Examination of the undamaged fracture face revealed features consistent with fatigue. The specialist reported that it is considered probable that the offset between the grooves in the threaded portion of the control cable are indicative of a torsional force being imparted during assembly. The torsion rotated the locking device during aircraft operation producing a loose connection which developed the fatigue. (The full Materials Laboratory report is attached to the public docket).

As a result of this accident, on August 13, 2008, MD Helicopters issued a mandatory service bulletin (SB) SB900-108R1, which required a non-destructive inspection of the cable threads by florescent magnetic particle, trimming the aft end of the control cable conduit, disposal of the locking device (which would prevent a repeat of the initial assembly error), drilling of a wire locking hole in the control tube, increasing the assembly torque, and wire locking of the control cable directly to the control rod. On August 14, 2008, the FAA issued an emergency airworthiness directive 2008-17-51, which repeated the requirements of SB900-108R1.

NTSB Probable Cause

The pilot's inability to maintain directional control due to the fatigue failure of the threaded portion of the forward directional control cable as a result of the improper installation a lock washer.

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