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N407MH accident description

Colorado map... Colorado list
Crash location 37.835000°N, 107.881667°W
Nearest city Telluride, CO
37.937494°N, 107.812285°W
8.0 miles away
Tail number N407MH
Accident date 03 May 2014
Aircraft type Bell 407
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On May 3, 2014 about 1130 mountain daylight time, a Bell 407 helicopter, N407MH, experienced an engine chip light followed by a loss of engine power. The pilot executed a forced landing to snow-covered mountainous terrain (above 10,000 ft MSL) near Telluride, Colorado. The commercial pilot and two crew members were not injured. The helicopter sustained substantial damage during the landing. The helicopter was registered to and operated by Classic Helicopters, Incorporated, of Odgen, Utah, on a company visual flight rules flight plan under the provisions of 14 Code of Federal Regulations Part 135 as a search and rescue flight. Visual meteorological conditions prevailed in the vicinity of the accident. The flight originated from Moab, Utah.

The pilot stated that they were conducting a search and rescue mission for the San Miguel Sheriff's Department, searching for a person who had been missing overnight. After flying 5 or 6 lines of the search grid, the pilot made a right turn to begin another line when there was change in engine noise. Almost immediately the engine chip detector light illuminated followed by a full authority digital engine control (FADEC) degrade light. The helicopter was about 200 ft AGL. The pilot started to descend toward an open snow-covered meadow for a landing, but the engine RPM degraded so he initiated an autorotation. The helicopter touched down with little forward airspeed, bounced, and the left skid became hung up on an object under the snow. The helicopter rolled onto its left side and came to rest. All three occupants exited without injuries.

AIRCRAFT INFORMATION

The helicopter was a Bell Helicopter Textron, Incorporated model 407, serial number 53100. It was configured for emergency medical use. The helicopter was powered by one Rolls Royce Incorporated M250-C47B turboshaft engine, serial number 847016, rated at 650 shaft horse power. The helicopter had undergone a 150 hour engine inspection on April 30, 2014. The airframe time at the inspection was 10,724.6 hours. The total airframe time recorded at the accident was 10,730.1 hours.

PILOT INFORMATION

The pilot, age 32, held a commercial pilot certificate with helicopter and instrument helicopter ratings. Additionally, the pilot held a flight instructor certificate with helicopter and instrument helicopter ratings. The pilot reported having 4,300 total flying hours with 740 hours in the make and model of the accident helicopter. He also reported having flown 42 hours in the 30 days preceding the accident. The pilot completed a flight review with his company on March 31, 2014.

The pilot reported having a second-class medical certificate dated April 22, 2014 with no restrictions or limitation.

WRECKAGE AND IMPACT INFORMATION

The left side of the helicopter passenger compartment showed inward buckling and skin wrinkles. Inward crushing damage was also observed to the upper rear engine cowling and engine exhaust. The lower left forward and lower right forward Plexiglas windows were broken out. The helicopter's tailboom was severed just aft of the main fuselage body. The tail rotor gear box was torn out at the end of the boom. The main rotor system remained attached at the mast and transmission. Three of the four main rotor blades were bent and broken. Part of the trailing edge of one blade was torn out. An examination of the helicopter's flight control system revealed no preimpact anomalies. A post-accident examination of the helicopter's engine showed the engine gas producer and power turbine drive train had continuity, but there was resistance to the gas producer and scraping of the power turbine when rotated. Additionally, ferrous debris was found in the engine scavenge oil filter. The helicopter's engine was removed and shipped to the engine manufacturer for further examination.

TESTS AND RESEARCH

The helicopter's engine was examined at Rolls Royce Corporation, Indianapolis, Indiana, on June 3-4, 2014. The examination showed that the power turbine thrust (No. 5) bearing was dry, gray/black in color, and heavily worn. The races and separator were in place, but no recognizable ball elements were present. The bearing and outer races were smeared with melted metal deposits. The ball separator was heavily scored with worn/enlarged ball pockets. The remaining power turbine components exhibited rotational contact damage consistent with a loss of radial and axial positioning, which is normally provided by the No. 5 bearing.

No. 4/5 Bearing Oil Jet

A small amount of oil was present underneath the No. 4/5 bearing oil jet at the gearbox port. The jet appeared to be in good condition. Unmetered alcohol was flowed through the jet at low pressure and exited the nozzle jets with no evidence of obstruction.

GEARBOX COVER OIL TRANSFER PASSAGE

Visual Inspection

Light directed into the gearbox cover oil delivery tube port was not observable at the passage exit. Unmetered alcohol squired into the passage did not pass through in either direction. The expected opening to the cast passage in the sidewall of the bore could not be observed under magnification or detected using a soft wire inserted into the port.

Radiographic Inspection

The gearbox cover was submitted for radiographic inspection. X-ray images revealed that the cover had been modified by a repair that included an insert being threaded into the oil delivery tube port. The insert was restricting the opening into the cast oil passage.

Oil Flow Test

A calibrated flow test of the gearbox passage using typical operating pressure and temperature settings was performed using a Rolls Royce production test bench. The initial test was performed with the 4/5 bearing oil jet installed. No measurable flow through the passage was produced. The piece was removed from the test bench and the No. 4/5 bearing oil jet was removed. The passage was ultrasonically cleaned. The cleaning produced some small particles consistent with coked oil and scarf. A second flow test performed using the same settings but without the 4/5 bearing oil jet installed produced a small amount of flow. The flow measured less than 2 percent of the No. 5 bearing 4/5 oil jet design flow specification.

Metallographic Examination

Measurements taken of the circumferential gap between the bottom of the threaded insert and the gearbox cover ranged from between 0.0005 and 0.005 inch. Deposits consistent with coked oil were observed in the cast oil passage adjacent to the circumferential gap.

ENGINE HISTORY RELEVANT TO THE GEARBOX COVER INSERT/OBSTRUCTION

The engine was manufactured in 1966. The gearbox cover, P/N23065470, serial number 44193, was original to the engine. The gearbox cover was marked with a material review board (MRB) symbol. The MRB record for the gearbox cover showed that a threaded insert was used as part of an oil transfer passage during original manufacture.

Gearbox Cover In-Service Exposure

The gearbox was disassembled seven times during its service life. No entry for additional gearbox cover oil delivery tube port repairs were found in the available service records. For additional information, see the Powerplant Group Chairman's Factual Report provided in the docket for this report.

NTSB Probable Cause

The failure of the power turbine thrust (No. 5) bearing due to overheating as a result of oil starvation, which led to the engine failure. Also causal to the accident was an undocumented repair to the gearbox cover oil delivery tube port during which an insert was threaded into the oil delivery tube port that subsequently restricted the oil flow to the power turbine thrust bearing.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.