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N37SV accident description

Florida map... Florida list
Crash location 25.997222°N, 80.221945°W
Nearest city Hollywood, FL
26.011201°N, 80.149490°W
4.6 miles away
Tail number N37SV
Accident date 12 Oct 2011
Aircraft type Socata Tbm 700
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On October 12, 2011, about 1334 eastern daylight time, a Socata TBM 700, N37SV, registered to SV Leasing Company of Florida, operated by SOCATA North America, Inc., sustained substantial damage during a forced landing on a highway near Hollywood, Florida, following total loss of engine power. Visual meteorological conditions prevailed at the time and an instrument flight rules (IFR) flight plan was filed for the 14 Code of Federal Regulations (CFR) Part 91 maintenance test flight from North Perry Airport (HWO), Hollywood, Florida. The airline transport pilot and pilot-rated other crewmember sustained minor injuries; there were no ground injuries. The flight originated from HWO about 1216.

The purpose of the flight was a maintenance test flight following a 600 hour and annual inspection.

According to the right front seat occupant, in anticipation of the flight, he checked the fuel load by applying electrical power and noted the G1000 indicated the left fuel tank had approximately 36 gallons while the right fuel tank had approximately 108 gallons. In an effort to balance the fuel load with the indication of the right fuel tank, he added 72.4 gallons of fuel to the left fuel tank. At the start of the data recorded by the G1000 for the accident flight, the recorded capacity in the left fuel tank was approximately 105 gallons while the amount in the right fuel tank was approximately 108 gallons.

The PIC reported that because of the fuel load on-board, he could not see the level of fuel in the tanks; therefore, he did not visually check the fuel tanks. By cockpit indication, the left tank had approximately 105 gallons and the right tank had approximately 108 gallons. The flight departed HWO, but he could not recall the fuel selector position beneath the thrust lever quadrant. He further stated that the fuel selector switch on the overhead panel was in the "auto" position.

After takeoff, the flight climbed to flight level (FL) 280, and levelled off at that altitude about 20 minutes after takeoff. While at that altitude they received a "Fuel Low R" amber warning CAS message on the G1000. He checked the right fuel gauge which indicated 98 gallons, and confirmed that the fuel selector automatically switched to the left tank. After about 10 seconds the amber warning CAS message went out. He attributed the annunciation to be associated with a failure or malfunction of the sensor, and told the mechanic to write this issue down so it could be replaced after the flight. The flight continued and they received an amber warning CAS message, "Fuel Unbalance" which the right fuel tank had more fuel so he switched the fuel selector to supply fuel from the right tank to the engine. The G1000 indicates they remained at that altitude for approximately 8 minutes.

He then initiated a quick descent to 10,000 feet mean sea level (msl) and during the descent accelerated to Vmo to test the aural warning horn. They descended to and maintained 10,000 feet msl for about 15 minutes and at an unknown time, they received an amber warning CAS message "Fuel Low R." Once again he checked the right fuel gauge which indicated it had 92 gallons and confirmed that the fuel tank selector automatically switched to the left tank. After about 10 seconds the CAS message went out. Either just before or during descent to 4,000 feet, they received an amber CAS message "Fuel Unbalance." Because the right fuel gauge indicated the fullest tank was the right tank, he switched the fuel selector to supply fuel to the engine from the right tank.

The flight proceeded to the Opa-Locka Executive Airport, where he executed an ILS approach which terminated with a low approach. The pilot cancelled the IFR clearance and proceeded VFR towards HWO. While in contact with the HWO air traffic control tower, the flight was cleared to join the left downwind for runway 27L. Upon entering the downwind leg they received another amber CAS message "Fuel Unbalance" and at this time the left fuel gauge indicated 55 gallons while the right fuel gauge indicated 74 gallons. Because he intended on landing within a few minutes, he put the fuel selector to the manual position and switched to the fullest (right) tank.

Established on final approach to runway 27L at HWO with the gear down, flaps set to landing, and minimum speed requested by air traffic for separation (85 knots indicated airspeed). When the flight was at 800 feet, the red warning CAS message "Fuel Press" illuminated and the right seat occupant with his permission moved the auxiliary fuel boost pump switch from "Auto" to "On" while he, PIC manually moved the fuel selector to the left tank. In an effort to restore engine power he pushed the power lever and used the manual over-ride but with no change. Assured that the engine had quit, he put the condition lever to cutoff, the starter switch on, and then the condition lever to "Hi-Idle" attempting to perform an airstart. At 1332:42, a flightcrew member of the airplane advised the HWO ATCT, "…just lost the engine"; however, the controller did not reply.

The PIC stated that he looked to his left and noticed a clear area on part of the turnpike, so he banked left, and in anticipation of the forced landing, placed the power lever to idle, the condition lever to cutoff, the fuel tank selector to off, and put the electrical gang bar down to secure the airplane's electrical system. He elected to retract the landing gear in an effort to shorten the landing distance. The right front seat occupant reported that the airplane was landed in a southerly direction in the northbound lanes of the Florida Turnpike. There were no ground injuries.

AIRCRAFT INFORMATION

The airplane was manufactured in 2008, by EADS Socata as model TBM 700, and was designated serial number 441. At the time of the accident, it was powered by a 850 horsepower Pratt & Whitney Canada PT6A-66D engine and equipped with a Hartzell HC-E4N-3/E9083 propeller with reverse capability.

The airplane's fuel system consists of a 150.5 gallon capacity wet wing fuel tank in each wing, with a resulting total usable capacity of 292 gallons. Fuel gauging is a capacitance type with 3 probes installed in each wing, and a low fuel sensor installed in each wing inboard of the inboard fuel probe, which provides a low level CAS messages when the fuel quantity remaining in the concerned tank is under about 9 U.S. gallons. The fuel probes are capacitors connected in parallel via electrical harness to the fuel amplifier (FCU) which in turn is connected electrically to the G1000 in the cockpit for display for the fuel tank readings.

Review of the maintenance records revealed an entry on August 4, 2010, indicating, "Troubleshoot right fuel quantity, found pin B at P61 connector loose, removed and replaced pin B at P61 connected as required, performed an operational check of right fuel quantity, system operates normal." The airplane total time at that time was recorded to be 451.1 hours. There was no other record of repair of the right fuel harness.

On September 29, 2011, the airplane was flown to HWO for compliance with an annual/600-Hour inspection. A pre-inspection engine run-up was performed and according to a fuel timeline provided by the maintenance facility, the reading for the fuel level in the right fuel tank at the completion of the run was recorded by the G1000 to be 41 gallons. On October 4, 2011, due to fuel leaking from 2 panels of the right wing, it was drained of fuel. A total of about 70 gallons of fuel were drained from the right fuel tank. The same day, electrical power was applied for about 43 seconds and during this time the right fuel quantity at the beginning and ending of the power-up was recorded to be approximately 11 gallons, though there was no remaining fuel in the fuel tank. The leaking panels were removed, repaired, and reinstalled. On October 5th, the fuel drained from the right tank were placed back into the right wing, and a post maintenance run-up was performed using only fuel from the right fuel tank. This was done in an effort to balance the fuel load. The G1000 recorded that at the completion of the engine run, the right fuel tank contained 51 gallons. The G1000 indicated power application 2 days later indicating the right fuel tank had approximately 143 gallons, despite the fact that it had not been fueled. Five days later, on October 12, 2011, the G1000 indicated power application for less than 30 seconds which indicated the right fuel tank had 107 gallons of fuel, while the left fuel tank had 35.5 gallons of fuel. No maintenance was done to evaluate the reason for the changing right fuel quantity.

Further review of the maintenance records revealed that the airplane was last inspected in accordance with a 600 hour inspection and annual inspection which was signed off as being completed the day before. The airplane total time at that time was recorded to be 593.4, while the airplane total time at the time of the accident was 595.2 hours.

FLIGHT RECORDERS

The airplane was equipped with a Garmin G1000 Integrated Flight Deck, which is a collection of multiple avionics units which include flight displays. Each display has two SD card slots. The SD memory card was removed from the MFD and sent to the NTSB Vehicle Recorder Division for readout.

According to the NTSB Factual Report, the data was extracted normally and contained 59 log files. The event flight was recorded and contained approximately 1 hour and 38 minutes of data; the calculated sample time interval was 1.055 seconds per data record. A review of the recorded data with respect to the fuel level revealed that beginning about 1218, or about 2 minutes after takeoff until 1229, during which time the airplane was at FL190 and climbing to FL280, the fuel level indication for the left steadily decreased consistent with supplying fuel to the engine, while the fuel level indication for right varied with increases noted. The left fuel level remained steady from about 1229 until about 1245, indicative of fuel being provided from the right fuel tank. From about 1245 until about 1324, a steady decrease of the left fuel quantity was noted, while during the same period the right fuel quantity indication showed a general decline. At the end of the recorded data, the left fuel quantity was approximately 62 gallons, while the right fuel quantity was approximately 60 gallons. A copy of the report and data is contained in the NTSB public docket.

WRECKAGE AND IMPACT INFORMATION

The NTSB did not immediately respond to the accident site; however, the NTSB did view the airplane during the recovery process. The approximate location of where the airplane came to rest was reported to be 25 degrees 59.845 minutes North latitude and 080 degrees 13.312 minutes West longitude, or approximately 4,338 feet and 94 degrees from the approach end of runway 27L (intended runway). The airplane was recovered for further examination. According to the recovery crew, fuel leakage was noted at the accident site; however, it was not determined what tank(s) the fuel leaked from, nor the amount of fuel leaked.

The airplane was formally inspected by NTSB on October 17 and 18, 2011. Also in attendance were representatives of the FAA, technical advisor from Daher-Socata, and Pratt & Whitney Canada. As first viewed, both wings and the horizontal stabilizer were removed. The fuselage was fractured circumferentially at frame 8.

Examination of the cockpit revealed the auxiliary fuel boost pump switch was in the "Auto" position, the manual fuel tank selector was in the "Off" position, and the fuel selector switch on the overhead panel was in the "Manual" position.

Testing of the airplane's fuel quantity indicating system was performed using the aircraft's battery for electrical power. The right wing which was empty of fuel was electrically connected while the wing was inverted. With the aircraft's battery power applied, the G1000 displayed red X's for fuel quantity for both sides. The G1000 indicated that the fuel used was 88 gallons, and the fuel remaining was 123 gallons. The left wing which was empty of fuel was then electrically connected in an upright position and with the aircraft's battery power applied, the G1000 displayed 108 gallons in the left wing on initial power up. The gallons decreased steadily over the next 10 minutes to 29 gallons when the test was terminated. The left and right wings were electrically connected in an upright position, and with aircraft's battery power applied, the G1000 displayed 33 gallons for the left fuel tank and the right fuel tank indicated red X's. With battery power applied and fuel selector switch on overhead panel in auto position, the G1000 displayed changing of the fuel selector position. The fuel sequencer was not in bypass; approximately 2 ounces of fuel were drained from the fuel sequence reservoir, which contained slight aluminum particles on the screen. With battery power applied, a fuel supply plumbed to the left wing root, and the fuel selector positioned to the left tank, fuel flow noted at the firewall fitting and no suction was noted at the right wing root fitting. With battery power applied, a fuel supply plumbed to the right wing root, and the fuel selector positioned to the right tank, fuel flow noted at the firewall fitting and no suction was noted at the left wing root fitting. The fuel amplifier was retained for further examination.

Examination of the left wing following fuel system testing revealed the fuel tank was breached, but there were no obstructions inside the fuel tank. The fuel tank outlet finger screen had a little fuzz material present. Both flapper valves were installed and noted to operate normally. The low fuel sensor, fuel probes, and electrical harnesses pertaining to fuel were noted to be installed correctly. The low fuel sensor, inner fuel probe, intermediate fuel probe, outer fuel probe, main fuel tank electrical harness, intermediate strap electrical harness, high and low fuel vent valves, and fuel check valve were removed for further examination.

Examination of the right wing following fuel system testing revealed the fuel tank was breached, but there were no obstructions inside the fuel tank. The fuel tank outlet finger screen had some debris. Both flapper valves were installed and operate normally. The low fuel sensor, fuel probes, and electrical harnesses pertaining to fuel were noted to be installed correctly. The low fuel sensor, inner fuel probe, intermediate fuel probe, outer fuel probe, main fuel tank electrical harness, intermediate strap electrical harness, high and low fuel vent valves, and fuel check valve were removed for further examination.

Cursory examination of the engine and propeller revealed all four propeller blades were bent aft. Rotation of the propeller by hand resulted in expected rotation of the power turbine assembly, while rotation of the compressor assembly resulted in expected rotation of all the Accessory Gearbox (AGB) drives. Examination of the fuel filter revealed the level of residual fuel in the bowl measured 0.400 inch. The propeller was removed from the engine which was removed from the airframe and shipped to Pratt & Whitney Engine Services (PWES) facility for engine operational testing.

Prior to operational testing of the engine with FAA oversight, borescope examination of it revealed no discrepancies. The engine was placed in a test cell as received and with FAA oversight, the engine was started and operated at various power settings for over 2.5 hours. Four parameters exceeded the Overhaul Manual tolerances for a zero time engine , but when the repair limits that factor in the engine's operating time were used, the only parameter out of tolerance was the inter turbine temperature (ITT), which can be adjusted with a trim class change. A copy of the report from the engine manufacturer is contained in the NTSB public docket.

TEST AND RESEARCH

According to the maintenance manual, a low level test, and indicator calibration on aircraft are not due until 1,500 hours and/or 4 years; therefore, these special inspection items were not performed during the last 600-Hour/Annual inspection.

According to section 3.8 of the Pilot's Operating Handbook (

NTSB Probable Cause

The pilot’s failure to terminate the flight after observing multiple conflicting errors associated with the inaccurate right fuel quantity indication. Contributing to the accident were the total loss of engine power due to fuel starvation from the right tank, the inadequate manufacturing of the right fuel gauge electrical harness, and failure of maintenance personnel to recognize and evaluate the reason for the changing fuel level in the right fuel tank.

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