Plane crash map Locate crash sites, wreckage and more

N1831W accident description

Georgia map... Georgia list
Crash location 31.642222°N, 82.609722°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect.
Nearest city Alma, GA
31.539370°N, 82.462356°W
11.2 miles away
Tail number N1831W
Accident date 04 Aug 2013
Aircraft type Beech A36
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On August 4, 2013, about 1155 eastern daylight time, a Beech A36, N1831W, was destroyed when it impacted trees and terrain near Alma, Georgia. Day, visual meteorological conditions prevailed and an instrument flight rules flight plan was filed. The private pilot and passenger were fatally injured. The personal flight was conducted under the provisions of Title 14 Code of Federal Regulations Part 91. The flight departed Fernandina Beach Municipal Airport (FHB), Fernandina Beach, Florida around 1115 with the intended destination of Gwinnett County Airport-Briscoe Field (LZU), Lawrenceville, Georgia, where the airplane was based.

A review of voice recordings provided by Jacksonville Air Traffic Control Tower (JAX) revealed no indication from the pilot of any anomalies. A radar hand-off was accomplished between JAX to Jacksonville Air Route Traffic Control Center (ZJX). The pilot contacted ZJK at 1127 and was issued the current altimeter setting. Then, at 1151, while en route at 5,000 feet mean sea level (msl), the airplane lost radar contact and the radar controller attempted to contact the pilot; however, no response was recorded or noted. A review of radar data indicated that the radar target began to descend from about 5,000 feet msl starting at 1150:52. The next radar targets were recorded at 4,900 feet msl at 1151:04, then 3,900 feet msl at 1151:16, and the last radar target was at 2,800 feet msl at 1151:28. The wreckage was located about 2 miles to the northwest of the last radar return.

Witnesses reported hearing a "low flying" airplane and soon after, the sound of impact. One witness went to the scene and notified the Sheriff's Department. The other witness stated that when he first heard the airplane it sounded like the engine was sputtering but it then straightened out.

PERSONNEL INFORMATION

According to Federal Aviation Administration (FAA) records, the pilot held a private pilot certificate with ratings for airplane single-engine land and instrument airplane. He held a third-class medical certificate, which was issued on January 13, 2012 and had a restriction of "must wear corrective lenses." At the pilot's most recent medical examination he had reported 601 total flight hours and 40 of those flight hours were in the 6 months preceding the medical application.

AIRCRAFT INFORMATION

According to FAA records, the airplane was issued an airworthiness certificate in 1973 and was registered to APS Aviation LLC on March 18, 2010. It was equipped with a Continental Motors IO-550-B(4) series, serial number 249169-R, 300-hp engine. It was also equipped with a McCauley propeller. The airplane's most recent annual inspection could not be documented due to the inability to locate the records at the time of this writing. A flight log form found at the accident site noted "Annual," dated July 8, 2013, at the tach time of 2764.9 hours.

The most recent recorded fueling was accomplished on August 4, 2013 at FHB. The airplane had been fueled with a total of 20 gallons of fuel; 10 gallons of fuel in each main fuel tank.

METEOROLOGICAL INFORMATION

The 1153 recorded weather observation at AMG, which was about 8 nautical miles to the southeast of the accident location, included wind from 290 degrees at 5 knots, 8 miles visibility, scattered clouds at 3,200 feet above ground level (agl) and 4,600 feet agl, temperature 31 degrees C, dew point 23 degrees C, and barometric altimeter 30.04 inches of mercury.

COMMUNICATIONS

A review of voice recordings provided by Jacksonville Air Traffic Control Tower (JAX) revealed no indication from the airplane of any anomalies. A radar hand-off was accomplished between JAX to Jacksonville ARTCC (ZJX). The accident flight contacted ZJK at 1127 and was issued the current altimeter setting. Then, at 1151, while en route at 5,000 feet mean sea level, the radar data tag for the accident airplane went into to a coast mode. The radar controller attempted to contact the accident flight; however, no response was recorded or noted.

WRECKAGE AND IMPACT INFORMATION

The airplane impacted 60-foot-tall trees beyond an open field and then descended until it impacted the ground at a wings-level, nose down attitude. The accident flight path was oriented on a 304 degree heading and the debris path began at the initial tree strike and continued about 650 feet in length.

Nose Section

The engine was separated from the engine mounts and located about 50 feet forward of the main wreckage. The engine cowling was separated from the engine and located along the debris path. The nose gear was impact separated from the keel structure of the airplane and located in the vicinity of the main wreckage. The propeller and spinner remained attached to the propeller flange. The propeller blades exhibited S-bending. There were several pieces of smoothly-cut tree branches located along the debris path. The branches exhibited paint transfers along the faces of the cuts similar in color to the propeller blades. The cuts were about 45 degree angles to the plain of the branch.

The engine remained attached to the firewall through wires but was separated from all of the engine mounts. All six cylinders remained attached to the crankcase. The No. 5 cylinder was impact damaged. Both magnetos were separated from the engine. The left magneto remained attached through the ignition harness and the right magneto was located along the debris field. The starter was separated from the engine and was located along the debris field. In addition, the alternator was impact fractured and several pieces were scattered throughout the debris field.

Right Wing

Sections of the right wing, right flap, and right aileron were scattered along the debris path. The inboard section of the right wing was located underneath the fuselage. The entire right wing exhibited impact crush damage. The flaps were impact separated at their respective attach points. Cable continuity was confirmed from the flap motor located near the cabin area to the actuators; however, they exhibited numerous tensile overload fractures. The aileron was separated from the wing and the aileron cables exhibited tensile overload at all fracture points; however, cable continuity was confirmed from the base of the control column to the associated fracture points out to the aileron. The right wing's main fuel tank fuel cap remained attached, was seated correctly, and locked in position in the forward right wing section located along the debris path. The right main landing gear was separated and discovered about 15 feet forward of the main wreckage. The right flap actuator was measured and corresponded to the flaps retracted position.

Empennage

The rudder remained attached to the vertical stabilizer. Cable continuity was confirmed from the base of the rudder pedals to the rudder through several cable fractures. All separations exhibited tensile overload signatures. All flight control surfaces associated with the tail section remained attached to their respective attach points; however, the empennage was separated from the fuselage. The left and right elevator counter weights were impact separated from the elevator and located along the debris path. Elevator cable continuity was confirmed from the base of the control column to the elevator bellcrank although numerous tensile overload fractures were present along the entire span. Both elevator trims were measured and correlated to a nose down trim position.

Left Wing

The left wing was found inverted and separated from the fuselage at the wing root. The wing exhibited extensive crush and impact damage along the entire span. The fuel tanks were breached, devoid of fuel, and the fuel caps remained secured and seated. The flaps remained attached at their respective attach points at the flap bell crank. Flap control continuity was confirmed for the flaps although the drive cable was separated from the flap motor assembly in tensile overload. The aileron was separated and cable continuity was confirmed from the base of the control column to the associated fracture points out to the aileron attach point. The aileron cable exhibited tensile overload at all fracture points. The landing gear actuator was discovered in the retracted position. The left main landing gear remained in the up and locked position. The left flap actuator was measured and corresponded to the flaps retracted position.

Cockpit

The cockpit exhibited extensive impact and crush damage. A Garmin 696 handheld global positioning system was located, which was removed and sent to the NTSB Vehicle Recorder Laboratory for download. The engine controls were separated from the cockpit and located in the vicinity of the main wreckage. The throttle lever and the propeller lever were in the mid-range position. The mixture was in the full forward position. Due to extensive damage, the levers were impact separated from their associated control cables. The tachometer indicated a time of 2778.16 hours. The vertical speed indicator needle was in the 400 feet per minute down position. The aileron balance cable was intact from the left bellcrank to the right bellcrank where it exhibited overload failure at the right aileron. The transponder was examined and the setting of the transponder could not be determined.

Fuselage

The fuselage came to rest about 600 feet from the initial tree impact point. It came to rest on the left side. The main cabin door was separated from the fuselage. The main cabin door latch was in the closed position. In addition, both the forward and aft utility doors were in the latched and closed position; however, both were impact separated from the fuselage. The pilot and co-pilot seats were impact separated from the cabin and located forward of the main wreckage. The aft seats remained attached to the cabin floor.

The fuel selector was located in the vicinity of the main wreckage. The fuel selector was located in the left main fuel tank detent. All of fuel fittings that attached to the fuel selector were finger tight. An odor similar to aviation fuel was noted when the fuel selector was disassembled. Residual liquid that was similar in odor to aviation fuel was noted in the fuel strainer with no debris noted in the fuel. Residual fuel was also noted in the fuel boost pump when it was disassembled. The fuel boost pump was in the "OFF" position.

MEDICAL AND PATHOLOGICAL INFORMATION

A postmortem examination of the pilot was performed by the Georgia Bureau of Investigation, Division of Forensic Sciences, on August 7, 2013. The autopsy report noted the cause of death as "multiple blunt force injuries" and the manner of death was "accident."

Forensic toxicology was performed on specimens from the pilot by the FAA Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma. The toxicology report stated no ethanol was detected in the muscle or liver. Atorvastatin and Doxazosin were detected in the muscle and liver. Azacyclonol, Fexofenadine, and Ibuprofen were detected in the liver. In addition, testing for carbon monoxide and cyanide was not performed due to the lack of a suitable sample.

No postmortem examination or toxicology tests were performed on the passenger.

TESTS AND RESEARCH

Engine Examination

The engine was examined at the manufacturing facility in Mobile, Alabama, on September 10-11, 2013. The oil filter and fuel filter were void of any debris. The spark plugs were removed, all exhibited normal wear, and were light gray in color. The starter adaptor, induction system, exhaust system, oil cooler, manifold valve, throttle body, oil sump, oil suction screen, and cylinders were removed, disassembled, and examined with no anomalies noted. In addition, the camshaft and crankshaft were removed and examined. Overall, examination revealed that there were no abnormalities with the engine that would have precluded normal operation.

ADDITIONAL INFORMATION

Portable Global Positioning System

A Garmin 696 portable global positioning system was located in the wreckage and sent to the NTSB Vehicle Recorders Laboratory for download. The data downloaded was for dates prior to the accident date and did not reveal any pertinent information regarding the accident flight.

NTSB Probable Cause

Descent from cruise flight until impact with trees and the ground for reasons that could not be determined because postaccident examination of the wreckage did not reveal any anomalies that would have precluded normal operation and the pilot's autopsy and toxicology tests did not provide any evidence of impairment or incapacitation.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.