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N58020 accident description

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Crash location 40.300000°N, 74.668611°W
Nearest city West Windsor, NJ
40.291775°N, 74.641269°W
1.5 miles away
Tail number N58020
Accident date 15 Sep 2012
Aircraft type Aerospatiale As 355F1
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On September 15, 2012, at 1200 eastern daylight time, an Aerospatiale AS 355F1, N58020, operated by Analar Corporation, was substantially damaged when it impacted terrain following an in-flight breakup near West Windsor, New Jersey. The commercial pilot was fatally injured. The positioning flight was conducted under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed for the planned flight to Atlantic City International Airport (ACY), Atlantic City, New Jersey. The flight originated from Princeton Airport (39N), Princeton, New Jersey, about 1155.

According to the owner and president of the operator, the helicopter had flown during the summer with a loaner main transmission, while its own transmission was sent out for repair. After the repair was complete, the helicopter's main transmission was received and then reinstalled on September 13, 2012. After the installation, the president conducted a maintenance ground run, followed by a 30-minute maintenance test flight, with no anomalies noted. Earlier during the day of the accident, the accident pilot completed a roundtrip flight uneventfully, with a relative of the helicopter owner onboard. Specifically, the pilot flew from 39N to the West 30th Street Heliport (JRA), New York, New York, picked up the passenger, and flew back to 39N. At the conclusion of that flight, the helicopter was "hot fueled" to its maximum fuel capacity and then departed on the accident flight to pick up another relative of the helicopter owner at ACY. The president estimated that the helicopter had flown approximately 1 hour 10 minutes since the installation of the transmission when the accident occurred.

According to information from the Federal Aviation Administration (FAA), the helicopter was in radio and radar contact with McGuire Approach Control. Radio and radar contact were lost at 1200 and no distress calls were received. Witnesses near the area of the accident site reported hearing a banging, explosion, or engine rev noise, followed by a piece separating from the helicopter and the helicopter spiraling nose down toward the ground.

PILOT INFORMATION

The pilot, age 65, held a commercial pilot certificate with ratings for airplane single-engine land, rotorcraft helicopter, instrument airplane and instrument helicopter. His most recent FAA second-class medical certificate was issued on July 21, 2012. It was a deferred issuance due to a new onset of atrial fibrillation. He was previously issued a second-class medical certificate on September 12, 2011. According to employer records, the pilot had a total flight experience of approximately 11,100 hours; of which, about 2,200 hours were in the same make and model as the accident helicopter. The pilot had flown about 21 hours during the 90 days preceding the accident.

AIRCRAFT INFORMATION

The six-seat helicopter, serial number 5227, was manufactured in 1982. It was equipped with two Rolls-Royce (Allison) 250-C20F, 420-shaft horsepower engines. The helicopter was maintained under a manufacturer's approved inspection program. It's most recent inspection was a 100-hour inspection, which was completed on the morning of the accident in conjunction with the installation of the repaired main transmission. At that time, the helicopter had accumulated 11,431.3 hours of operation. The helicopter's most recent 600-hour inspection was completed on June 5, 2012. At that time, the helicopter had accumulated 11,332.7 hours of operation.

METEOROLOGICAL INFORMATION

Trenton Mercer Airport (TTN) was located about 7 miles west of the accident site. The recorded weather at TTN, at 1153, was: wind 350 degrees at 9 knots, gusting to 16 knots; visibility 10 miles; sky clear; temperature 21 degrees C; dew point 9 degrees C; altimeter 30.14 inches Hg.

WRECKAGE INFORMATION

The helicopter came to rest upright in a cornfield, on a magnetic heading of 305 degrees. A postcrash fire consumed a majority of the cockpit and cabin. Due to fire damage, flight control continuity could not be confirmed. Both antitorque pedals were installed. The right cyclic was installed and the left cyclic was located in the field next to the rotorhead, consistent with its removal prior to flight. The right collective was installed and fire damaged. The left collective was not recovered. The majority of the instrument panel, including the caution warning panel, was consumed by fire. Three identifiable engine instruments were recovered; however, their indicating needles were loose. One front seat buckle was identified and noted as unclasped. Both forward cabin doors were found about 50 yards from the main wreckage. The doorpost and segments of the windshield remained attached to the right door. The doorpost and windshield were found separated from the left door (for more information, see Wreckage Plot in the public docket).

The aft section of tailboom was not consumed by fire and exhibited impact damage. The right horizontal stabilizer was separated near the root and a segment of the right horizontal stabilizer was recovered about 165 yards southeast of the main wreckage. The separation signatures were consistent with main rotor blade contact. The left horizontal and upper vertical stabilizers remained attached and were undamaged. The ventral fin remained attached; however, the lower end of the fin sustained impact damage. The tailboom had separated forward of the horizontal stabilizer. The tailrotor driveshaft remained intact from the tailrotor gearbox to just prior to the forward spline, where the tailrotor driveshaft had melted. One tailrotor blade remained attached to the tailrotor hub. The other tailrotor blade separated at the hub and was found 25 yards north, consistent with impact damage. The left engine cowling, with its intake screen, was located about 140 yards south of the main wreckage. The cowling was coated with clean (light yellow/brown) oil on both sides.

The rotorhead, located about 100 yards southwest of the main wreckage, included the top portion of transmission (the conical housing with the epicyclic and ring gear attached), the main rotor shaft, the starflex, and the red and blue main rotor blades with their sleeves and spherical thrust bearings attached. Also included were two servos (left-roll and right-roll) and three pitch change rods. A third servo (fore/aft) was found near the rotorhead, but had separated at both rod end connections; both upper and lower rod end bearings remained attached to the stationary swashplate and conical housing, respectively. The entire yellow main rotor blade and sleeve assembly had separated from the rotorhead and was later recovered about 270 yards southeast of the main wreckage. The yellow star arm had separated from the starflex and was located about 40 yards south of the main wreckage. The lower (stationary) scissor link assembly separated from both hinges and was not recovered. The rotorhead had separated from the main transmission near the upper flange of the bevel gear reduction module's cylindrical housing; the fracture surface remained intact with the separated rotorhead (for more information, see Airworthiness Group Chairman Factual Report in the public docket).

Metallurgical examination of the retained components revealed that the upper rod end of the fore/aft servo (actuator) remained attached to the swashplate and exhibited a bending overstress fracture near its neck. The lower threaded end of the upper rod end (shank, nut, and lock washer) was not in the actuator and was not recovered. The mating threads of the fore/aft servo upper end fitting exhibited severe wear, consistent with thread wear occurring over a period of time. The upper end fitting was packed with soil, consistent with its exposure prior to ground impact. Additionally, new thread impressions were observed, below the original worn threads, consistent with a vibration of the shank in the actuator hole. Metallurgical examination of all other retained components did not reveal any preimpact mechanical malfunctions (for more information, see Materials Laboratory Factual Report in the public docket.)

Evidence of Mastinox, a corrosion inhibiting compound, was found on the threaded shank of the left-roll and right-roll servo’s upper rod end (threaded shank of fore/aft servo upper rod end not recovered). Evidence of Mastinox was not found on the remnant upper rod end and end fitting of the fore/aft servo; however, the operator reported that they used Mastinox for the servo connections due to the dissimilar metals (aluminum and steel) and covered the Mastinox with a "thin" layer of grease. No evidence of grease was observed on the servo rod ends or fittings. For the servo rod ends’ threaded connection, the Eurocopter maintenance manual (MM) listed only G.355 grease and did not prescribe for the use of Mastinox. However, the Eurocopter standard practices manual stated that a torque correction factor of 0.4 was used for G.355 grease, but not for Mastinox. According to a representative from Eurocopter, the torque value listed in the manual for the rod ends already took the torque correction factor into account and a higher torque would have been necessary when Mastinox was used in place of G.355 grease. The operator reported that they did not adjust torque factor when using the Mastinox with a "thin" layer of grease. Additionally, evidence of sealant at the junction of the upper rod end and nut was not found on either the left-roll or right-roll servos (the sealant area on fore/aft servo was not recovered for inspection). Maintenance procedures for the installation of the rod ends of the servo-controls were found in the Eurocopter Maintenance Manual (MET) Work Card (WC) 67.30.15.401. Review of the WC revealed "…Apply a bead of sealant on the nut (8) and the thread of the ball end (1)…"

MEDICAL AND PATHOLOGICAL INFORMATION

An autopsy was performed on the pilot by the Mercer County, Office of the Chief Medical Examiner, West Trenton, New Jersey, on September 17, 2012. The cause of death was noted as "Massive multiple traumatic injuries." Toxicological testing was performed on the pilot by the FAA Bioaeronautical Science Research Laboratory, Oklahoma City, Oklahoma. Review of the toxicological report revealed:

"Metoprolol detected in Blood"

ADDITIONAL INFORMATION

Fore/Aft Servo

The Air Equipment F6103 31026-010 (serial number 68) fore/aft servo was manufactured in 1981 and installed on the accident helicopter in 1994. It's most recent overhaul was completed by Aerocopter Component Services (ACS), Ontario, Canada, in March 2008. In August 2010, the fore/aft servo was repaired by ACS and recertified to manufacturer specifications in accordance with Air Equipment Component Maintenance Manual (CMM) No. 67-39-10. Specifically, a bearing was replaced due to play in the pilot valve. In November 2011, the fore/aft servo was again repaired by ACS and recertified to manufacturer specifications in accordance with the same CMM. During the second repair, items were replaced due to hydraulic fluid seepage. A manager at ACS stated that during the most recent repair, the threads were inspected per the CMM and no discrepancies were observed at that time. Review of the CMM revealed, "…check all male and female threads for general condition…"

Review of MET WC 05.21.00.603, titled "Daily Operating Checks" (after last flight of day) revealed, "Servocontrols, hydraulic system. Security, absence of leaks, lines."

Review of MET WC 05.23.00, titled "Basic Inspection" (T Inspection/600-hour Inspection), section 6.3, revealed:

"Servo-controls and particularly rod end bearings

(Fig. 1, DETAIL B) :

Disconnect a mounting pin (W.C. 67.30.00.402 or 67.30.15.402).

Manually check that radial play (J) is normal, the second anchoring point being used as fulcrum. J

If in doubt, remove servo-control as per W.C. 67.30.00.402 or 67.30.15.402 for check in workshop.

Connect or install servo-control as per W.C. 67.30.00.402 or 67.30.15.402."

While the Basic T/600-hour inspection called for checking radial play of the rod end bearings, there was no specific guidance to check either the security (torque) of the rod end nut to the servo end fitting or to inspect the condition of the threaded connection. Review of Eurocopter Standard Practices Manual W.C. 20.02.05.404 contained general guidance for the inspection of threaded components, which must be performed each time an externally threaded part is removed. Other than the note in the daily operating check to look for security and absence of leaks, there was no other guidance specifically pertaining to the security of the rod end connection to the servo end fitting.

NTSB Probable Cause

Disconnection of the upper rod end from the fore/aft servo due to severely worn threads, which resulted in a loss of control and separation of a main rotor blade during cruise flight. Contributing to the accident were incorrect maintenance procedures and inadequate maintenance inspections performed by the operator, and insufficient inspection criteria provided by the helicopter manufacturer.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.