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N339NG accident description

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Crash location 40.431667°N, 80.034444°W
Nearest city Pittsburgh, PA
40.440625°N, 79.995886°W
2.1 miles away
Tail number N339NG
Accident date 17 Mar 2011
Aircraft type Bombardier Inc Dhc 8 402
Additional details: None

NTSB Factual Report

HISTORY OF THE FLIGHT

On March 17, 2011, about 1640 UTC, a Colgan Air DeHavilland DHC-8-400Q, N339NG, powered by two Pratt & Whitney Canada (PWC) PW150A turboprop engines, made a precautionary landing after experiencing an engine casing burn-through. The airplane was operating under the provisions of 14 Code of Federal Regulations Part 121 as scheduled passenger service from Cleveland Hopkins International Airport, Cleveland, Ohio (CLE) to Baltimore-Washington International Airport, Baltimore, Maryland (BMI). The flight crew reported that, during cruise flight at FL230, the left engine oil pressure master warning activated and the left engine oil temperature rapidly increased. The left engine lost power and the engine fire warning activated. The flight crew declared an emergency and the flight was diverted to Pittsburgh International Airport (PIT), where a single-engine landing was performed without incident. There was minor damage to the airplane, and no injury to the two flight crew, two cabin crew, and 36 passengers. A post-flight airplane inspection found a hole in the left engine gas generator case. The left engine and the two left nacelle Kidde Aerospace & Defense UTC (KAD) pneumatic fire/overheat detection elements were removed for further investigation.

AIRCRAFT INFORMATION

At the time of the incident, the airplane and the engine had accumulated 551 hours and 551 cycles since new. A review of the Colgan Air airplane maintenance records found no discrepancies.

AIRCRAFT DAMAGE

There was minor scorching damage to the airplane's left nacelle.

RECORDERS

The airplane was equipped with a digital flight data recorder (FDR) and two engine monitoring units (EMUs). Data extracted from the FDR and the left engine EMU showed that a left engine oil system (chip detector) fault was recorded about 20 minutes after takeoff and that the left engine oil pressure master warning activated about five minutes later (T+0). The data also showed that the left engine flamed out 82 seconds after activation of the left engine oil pressure master warning (T+82), the left engine power lever was retarded at T+85, and the airplane fire detection system left engine nacelle fire/overheat warning activated at T+90. The left engine power lever was further decreased to FLIGHT IDLE at T+98. Fuel to the left engine was shut off (condition lever moved to FUEL OFF) at T+114.

FIRE

Both left nacelle fire suppression bottles were fired. After landing, airport fire and rescue personnel responding to the aircraft determined that no fire was present in the left nacelle. The left nacelle fire warning remained active until airplane power was shut down. A single burn-through hole was noted at the bottom of the left engine gas generator case. The nacelle and the engine showed scorching damage consistent with exposure to elevated temperatures. There was no evidence that molten metal spray or torching flame had emanated from the engine.

TESTS AND RESEARCH

The engine was examined at a PWC facility in St-Hubert, Quebec. There was an approximately 3.5-inch (axial) by 4.5-inch (circumferential) burn-through hole in the gas generator case axially in line with the engine diffuser pipe exit ports at 6 to 7 o'clock. The edges of the hole were irregular and charred, with deposits of molten material characteristic of a fire burning through the case wall from the inside. There was minor thermal damage to some of the engine external components in the vicinity of the hole. The engine oil was heavily contaminated with metal particles. The oil pump was seized and the oil pump drive shaft was separated at its calibrated shear point. The No. 1 (power turbine rotor rearward thrust support) bearing was destroyed; its outer race (OR) and its retention hardware were loose, the inner race (IR) and ball elements were heavily worn and heat-discolored, and the cage and OR were fractured. Metallurgical examination of the bearing fracture surfaces found that the OR had failed in fatigue from a crack initiating in a spalled area on the center of the raceway. The advanced stage of the raceway component deterioration and the loose OR retention hardware indicated that the cage and OR had fractured late in the failure sequence. Due to the severe damage, the root cause of the spalling could not be determined.

PT damage. Aft surfaces of the PT rotor assembly were rotationally scored and torn; the damaged parts included the No. 1 and No. 2 bearing retention hardware, several No. 7 bearing components, and the PT stage 2 blade trailing edges. Stationary structures just aft of the damaged rotor parts exhibited corresponding circumferential damage signatures.

Dry bearing cavities. The Nos. 4 and 5 main bearings exhibited the dull gray coloration, destroyed bearing elements, and wear damage characteristic of operation without adequate lubrication. All of the bearing cavities were dry. The remaining main engine bearings were dry, but intact.

Thermal damage. The No. 5 bearing area was extensively damaged. The No. 5 bearing housing assembly was thermally destroyed. The No. 5 bearing (titanium alloy) flexible support housing and the No. 5 bearing front carbon seal and cover were partially consumed/melted together and were no longer recognizable. The No. 5 bearing front air seal runner was scorched and the runner section was eroded/missing. The No. 5 bearing oil nozzle housing, housing outer cover, rear carbon seal, and outer race were severely heat damaged. The No. 5 bearing IR, OR, and cage were intact but were thermally damaged, and the rollers were disintegrated. The No. 5 bearing pressure and scavenge oil tubes were largely consumed. The integral diaphragm section of the gas generator diffuser assembly, a thin-walled titanium-alloy structure linking the No. 5 bearing support housing diameter with the gas generator shield at the diffuser apex diameter, was entirely consumed. Large sections of the combustion section large exit support duct (LESD) inner and outer walls were thermally consumed/melted. The thermal damage exposed the back face of the (titanium-alloy) impeller, which showed a rough and eroded surface texture and exducer vane tip erosion, but was otherwise intact. The three diffuser exit ducts located bearing at 6 to 7 o'clock and immediately inboard of the gas generator case burn-through hole were thermally consumed/melted. Diffuser ring bore inside surfaces exposed at the apex end of two of the melted exit ducts were in good condition. The remaining 20 diffuser exit ducts located around the circumference of the gas generator case were intact. The HPT front cover was partially oxidized and the HPT airfoil tips and leading edges were eroded. The gas generator case exhibited no significant thermal damage other than the burn-through hole at 6 to 7 o'clock. Re-solidified metal splatter was fused to the diffuser, diffuser exit ducts, LESD outer wall, combustion chamber inner liner and small exit duct, HPT disk nozzle housing assembly, HPT disk bore, HPT shroud segments, LPT airfoils and LPT shroud segments. The engine exhibited no circumferential melting damage or other evidence of high-velocity, 360 degree distribution of molten particles.

Left oil pump failure investigation. Teardown of the seized engine oil pump found that a vane in the pump element that scavenges oil from the engine's No 2/2.5 bearing cavity had not fully retracted due to metal contamination. The protruding vane struck the element rotor and arrested pump rotation, causing torsional overload separation of the pump driveshaft and cut-off of oil supply to the engine.

Nacelle pneumatic fire/overheat detection elements. Examination of the KADS pneumatic fire/overheat detection elements removed from the left nacelle found that one of the elements was stuck in the alarm state. The element was unable to return to the non-alarm state because of a permanently deformed detector switch diaphragm. The investigation also found that KAD pneumatic fire/overheat detection element detector switch diaphragms had failed to reset after activation during other DHC-8 series 400 airplane fire events.

ADDITIONAL INFORMATION

PWC's analysis of the titanium fire included an examination of a No. 5 bearing seal runner and No. 5 bearing flexible support removed from a non-fire damaged PW150 engine that had operated without oil pressure for a similar period of time as the Colgan engine, but at a lower power setting. Dimensional checks of the No. 5 bearing seal runner showed that it was radially deformed (coned) sufficient to permit contact with the No. 5 bearing flexible support during operation. The thin-walled sections (ribs) of the titanium alloy No. 5 bearing flexible support exhibited rubbing and erosion consistent with oxidation. Examination of the No. 5 bearing seal runner found microstructure consistent with exposure to excessive temperatures during operation. According to PWC, No. 5 bearing seal runner material properties can be exceeded when the No. 5 bearing cavity temperatures are abnormally elevated.

Airplane operating instructions for engine oil pressure loss. The DHC Q400 Quick Reference Checklist (QRC) states that indicated oil pressure below 44 psi or continuous illumination of an engine oil pressure warning light requires the flight crew to complete the QRC ENGINE FAIL/FIRE/SHUTDOWN (engine shutdown) checklist.

NTSB Probable Cause

the flight crew's delay in shutting down the left engine following an engine oil pressure master warning, which led to a hard rub inside the engine that served as an ignition point for a titanium fire. Contributing to the event was a PW150 No. 5 seal design vulnerability to titanium ignition that can occur with continued engine operation following an engine oil pressure loss event.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.